ligo-ex ligo-ds
  Richardson Lab Experimental Log, Page 8 of 10  Not logged in ELOG logo
New entries since:Wed Dec 31 16:00:00 1969
ID Date Author Typedown Category Subject
  430   Tue Aug 27 18:37:40 2024 LukeUpdateInterferometer SimulationsRingheater model update
Updated the model to produce a more circular deformation in the HR surface. The first three attachments are from irradiance patterns gotten from ray tracing. The last is from a pre-defined irradiance pattern.
Attachment 1: Initial_1W.png
Initial_1W.png
Attachment 2: Increased_rays_100W.png
Increased_rays_100W.png
Attachment 3: Increased_rays_more_100W.png
Increased_rays_more_100W.png
Attachment 4: Initial_100W.png
Initial_100W.png
  431   Thu Aug 29 16:39:34 2024 LukeUpdateVACPhotos of heater tape
Attachment 1: IMG_2052.jpeg
IMG_2052.jpeg
Attachment 2: IMG_2051.jpeg
IMG_2051.jpeg
Attachment 3: IMG_2048.jpeg
IMG_2048.jpeg
Attachment 4: IMG_2047.jpeg
IMG_2047.jpeg
Attachment 5: IMG_2046.jpeg
IMG_2046.jpeg
Attachment 6: IMG_2044.jpeg
IMG_2044.jpeg
  432   Sun Sep 1 16:17:40 2024 LukeUpdateVACVacuum chamber leak checking and re-applying heating tape

[Luke, Luis, Cinthia, Michal, Tyler]

On the 26th Cinthia, Michal, and I took off the insolation on the vacuum chamber and re-routed it to include the new RGA volume. 

The next day Luis and I finished up the last of the flanges to be attached. We attached the Pirani gauge with a conical reducing nipple to the 2.75" port on the vacuum chamber. We then preformed the Helium leak testing, both flanges were quite low the 2.75" flange had a leak of 1.68e-10 torr and the 1.33" flange of 5.5e-12 torr. The leak on the 1.33" flange was so low it was difficult to know how much of it was real and how much was just noise.

  433   Tue Sep 3 15:52:56 2024 LukeUpdateVACHeater tape initilization

[Luke, Tyler, Jon]

On the 3rd we set up the pid controllers for the heater tapes and after putting on the insulation we started heating them up. We first brought it to ~50C and let it stabilize, there was about a 6-7 degree difference between the RGA and the barrel temperature, with the barrel being higher. We then brought it to 60 then 70C it still maintained the slight difference between the RGA and barrel temperatures.

Here is a table of the temperatures of the flanges connected to electronics as I left it.

Electronics Temperature (C)
Pressure gauge (Main volume) 58
Main turbo pump 45
RGA 37
Pressure gauge (RGA volume) 39
Cal leak 40
Mini tubo pump 36
Pirani gauge 37

Notes: I removed the electronics from the pressure gauge (main volume) because while it was below the required threshold it was still quite high compared to the other flanges.

  434   Tue Sep 3 18:24:17 2024 TylerUpdateCDSCymac Timing Chassis Issue
[Tyler, Jon]

The timing chassis used for the cymac has been shut off due to an unknown issue causing its supplied current to fluctuate. All real-time models will be suspended until a solution is found.

  435   Fri Sep 6 14:34:52 2024 Luke UpdateVACHeating tape work

On the 5th I had tried to start baking the vacuum chamber however certain parts of the chamber were getting too hot and causing the controllers to shut off. So I turned them off so that the next day I could rearrange the temperature probes. I then on the 6th set them up so that instead of overshooting the temperature they would be a little low in places.

After being left over night the cooler parts of the vacuum chamber got much closer to the desired temperature of 120C.

Here is a table of the temperatures of the sections of the chamber. Note: After these measurements were taken the PID controllers were set to 125C.

Location   Temperature (C)
Lid (PID controller 1 emergency shutoff) 108
Barrel lower (PID controller 1) 120 
Barrel upper (PID controller 2 emergency shutoff) 118
RGA volume (PID controller 2) 120

Here is a table of temperature of the flanges that have electronics.

Electronics Temperature (C)
Pressure gauge (Main volume) 79
Main turbo pump 64
RGA 51
Pressure gauge (RGA volume) 55
Cal leak 47
Mini turbo pump 50
Pirani gauge 45 

Other temperatures of note:

The optical table was about 38C

The cleanroom was around 33C (~91F)

  436   Mon Sep 9 12:36:45 2024 MichaelUpdateInterferometer SimulationsUpdate on Analysis of Mode Mismatch Minimization in A#
I have taken a closer look at the solution curve in the mirror parameter space which I have searched, focusing on the "resilience" of specific points, with the plan to analyze how certain conditions of the interferometer change as we move along this solution curve.
Attachment 1: SRC_Mode_Mismatch_Update_9_9_24.pdf
SRC_Mode_Mismatch_Update_9_9_24.pdf
  438   Mon Sep 9 21:02:37 2024 LukeUpdateVACSteadystate temperature of flanges

I measured the temperature of the flanges and reconnected the RGA turning on its filament. I then turned off the PID controllers.

Here is a table that has the temperature of the different parts of the vacuum chamber.

Electronics Temperature (C)
Pressure gauge (Main volume) 81
Main turbo pump 67
RGA 53
Pressure gauge (RGA volume) 60
Cal leak 48
Mini tubo pump 46
Pirani gauge (1.33") 46
conical nipple (2.75") 82
Lid 112
Barrel lower 125
Barrel upper 122
RGA volume 125
Bottom of chamber 117
  439   Mon Sep 16 07:28:16 2024 LukeUpdateInterferometer SimulationsRing heater update
Attachment 1: 20240916_Ringheater_updates.pptx
  440   Mon Sep 16 13:51:23 2024 Luis MartinUpdateVACRGA Scans

[Luis, Luke}

Three RGA scans were taken. The improvement in the amount of HC in the vacuum is visible across the different measurements. Images are attached.

Attachment 1: 2024-09-11_PostBake1_ArO.png
2024-09-11_PostBake1_ArO.png
Attachment 2: 2024-09-13_PostBake1_ArO.png
2024-09-13_PostBake1_ArO.png
Attachment 3: 2024-09-16_PostBake1_ArO.png
2024-09-16_PostBake1_ArO.png
  442   Mon Sep 16 14:59:51 2024 TylerUpdateTCSFLIR RIN Update 09/16

Below is the dark noise spectrum of the Red Pitaya, which was measured over the course of a weekend. Additionally, I have successfully measured a signal from the photodetectors with the FROSTI as the IR source, so it seems there shouldn't be any worry of these particular detectors not being feasible for the RIN measurement.

Attachment 1: adc_noise_floor_photodectors.png
adc_noise_floor_photodectors.png
  443   Mon Sep 16 15:18:59 2024 Cynthia UpdateInterferometer Simulationsa breakdown of FROSTI and thermal effects and the resulting cavity scan
Attachment 1: ligo_update_9_16_(1).pdf
ligo_update_9_16_(1).pdf
  444   Mon Sep 23 08:29:49 2024 LukeUpdateInterferometer SimulationsRingheater update

Ringheater Update

If the link does not work here is the file.

Attachment 1: 20240923_Update.pptx
  446   Mon Sep 23 15:00:41 2024 Cynthia UpdateInterferometer Simulationscorrections on assumption for O5 coating
The document recording ETM07 and ETM08 coating (T2300093) was discussed: the current plume files are not necessarily correct in a way that LIGO lab have tried to add it on uncoated ETM such as ETM07 and it does not match what the coated ETM07 would look like. the plume should be added on top of the uncoated ETM instead of assuming an ideal ETM. According to Garilynn, the imperfection on uncoated ETM matters. So far the possible ETM data used for O5, ETM 11,14,19, and 20 are all uncoated, and different ways could be used to predict the plume, including the plume data on LIGO dcc or subtract the uncoated data from the coated for O4 ETM and use that as another guessed plume.
Attachment 1: Uncoated_S1_ETM07-v2.pdf
Uncoated_S1_ETM07-v2.pdf
  447   Mon Sep 23 15:11:21 2024 TylerUpdateScripts/ProgramsEffective Emissivity Analysis and RIN Update

A quick update on the effective emissivity analysis for the CIT FROSTI testing:

I was able to (roughly) match the OPD data to a referenced COMSOL model, with an applied power of 12.6 W (as seen below). However, when changing the emissivity of the ETM in COMSOL, the dT profiles do not seem to change much. I am not sure as to why this is the case at the moment, and will continue to look further.

Additionally attached are the current RIN measurements of the FROSTI prototype. Shown is the PSDs of both channels, in reference to their individual backgrounds.

Attachment 1: OPD_Plot.png
OPD_Plot.png
Attachment 2: Temp_emiss_plot.png
Temp_emiss_plot.png
Attachment 3: rin_photodectors.png
rin_photodectors.png
Attachment 4: RIN_setup.jpg
RIN_setup.jpg
  448   Wed Sep 25 09:06:09 2024 Luis MartinUpdateVACRGA Scans
RGA Scan Comparison

The following images compare the RGA scans from 9/23/24, after the first bake with the new vacuum system, with those from 3/14/24, after bake 12 with the old system.

The first image shows a graph of the raw data and includes the calibrated leak for both curves. As we can see, our new system meets LIGO standards of cleanliness.

The second graph contains the plot of the normalized data.

Attachment 1: 24overlay.png
24overlay.png
Attachment 2: 24overlayNormalized.png
24overlayNormalized.png
  Draft   Tue Oct 1 19:41:23 2024 ShaneUpdateCDSCyMAC Timing Chassis Issue
[Shane, Luis] Summary of the issue we've been having with the timing chassis: when we connect only the Valon 5015 to power, the timing signal comes out of it sinusoidal as expected and the status lights are steady and all looks good. As soon as we connect the 3010 to power, the signal (both coming out of the 5015 and coming out of the 3010) go flat and the status lights of the 5015 start to flicker. We think what may be going on is that the 5015 is drawing just enough power to survive on its own, but when the current gets split to go to the 3010 as well, the 5015 takes more than it needs and becomes overpowered, and thus no longer outputs anything. We want to test further by powering them with two separate power supplies, but we need another one of the power connectors for the 3010 (the only one we have branches out from the connector to the 5015 and we don't want to cut any of the wires). Images of the inside of the chassis, along with two roughly sketched circuit diagrams (one showing the current setup, in which they're powered by the same source, and one showing a possible test set up, in which they're powered separately.
Attachment 1: IMG_5917.jpeg
IMG_5917.jpeg
Attachment 2: IMG_5803.jpeg
IMG_5803.jpeg
Attachment 3: IMG_5804.jpeg
IMG_5804.jpeg
  452   Wed Oct 2 12:05:42 2024 Luke Update Ringheater modeling Update

Power point slides

  453   Wed Oct 2 12:20:43 2024 TylerUpdateTCSUpdated FROSTI Analysis 10/02/2024
Attached below are updates on current FROSTI prototype analysis.
Attachment 1: FROSTI_Analysis_Updates.pdf
FROSTI_Analysis_Updates.pdf
  454   Wed Oct 2 13:38:00 2024 CynthiaUpdateInterferometer Simulationscavity scan with averaged O4 ETM coating as plume
Attachment 1: O5plumevsCoating.png
O5plumevsCoating.png
Attachment 2: O5CoatAvgpt5.png
O5CoatAvgpt5.png
Attachment 3: O5AVgcoatingFROSTIpt5.PNG
O5AVgcoatingFROSTIpt5.PNG
  455   Wed Oct 2 14:49:59 2024 LiuUpdate FROSTI ETM actuation
Proposed FROSTI ETM actuation on the HOM7 resonance. Animation
  456   Thu Oct 3 19:35:04 2024 ShaneUpdateCleanroomCleanroom cleaning and particle count
[Luke, Michael, Cynthia, Mary]

cleaning cleanroom and particle count

  • 12:25 pm: started particle count
    • zone 3:
      • 0.3 u: 4614
      • 0.5 u: 872
      • 1.0 u:83
    • zone 4:
      • 0.3 u: 2411
      • 0.5 u: 415
      • 1.0 u: 83
  • 12:48 pm: began surface check and wipedown, including softwalls
  • 1:20 pm: started vacuuming the floor
  • 1:30 pm: finished vacuuming the floor
  • 1:34 pm: started mopping the floor
  • 1:40 pm: finished mopping the floor
  • 1:40 pm: started cleaning the buckets
  • 1:42 pm: started mopping with IPA wipes
  • 1:50 pm: finished mopping with IPA wipes
  • 1:51 pm: changed sticky floor mats
  • 3:44 pm: started particle count
    • zone 3:
      • 0.3 u: 3207
      • 0.5 u: 624
      • 1.0 u: 83
    • zone 4:
      • 0.3 u: 916
      • 0.5 u: 83
      • 1.0 u: 0
  457   Wed Oct 9 13:52:31 2024 TylerUpdateTCSRIN Update 10/09/2024

I tried adjusting the gain settings on the photodetectors to check if this would help improve the RIN spectra measurements. Overall, it doesn't look like it does, and if anything, looks worse. I assume this is so because as the gain is lowered, the amount of detectable signal from the FROSTI becomes smaller and smaller.

Attachment 1: RIN_plots_CH0.pdf
RIN_plots_CH0.pdf
  458   Tue Oct 15 15:27:38 2024 Xuesi MaUpdateELOGTiming Chassis Update

I conducted separate tests on the '5015' and '3010a'. When powered individually, the '5015' outputs a signal at 33.55 MHz with an amplitude of 608 mV. It draws 1 A of current from the power source. The input signal for the '3010a' is 33.54 MHz with an amplitude of 670 mV (peak-to-peak) and a 15 mV DC offset. The output signal from channel 1 is a 65.5 kHz square wave with an amplitude of 3.28 V. The '3010a' draws 0.1 A of current.

Both the '5015' and '3010a' work fine when powered separately. However, when both are powered together, the power source behaves as if there is a short circuit. The current theory is that the switch or breaker is tripping, as it has a 1 A current rating. Since the combined current demand of both devices exceeds 1 A, this may be causing the issue.

Slides for 10/16/2024 Group Meeting

Attachment 1: 20241015_134152.mp4
Attachment 2: 20241015_133118.png
20241015_133118.png
Attachment 3: 20241015_133124.png
20241015_133124.png
Attachment 4: 20241015_133136.png
20241015_133136.png
Attachment 5: 20241015_133207.png
20241015_133207.png
Attachment 6: 20241015_133543.png
20241015_133543.png
Attachment 7: 20241015_133550.png
20241015_133550.png
Attachment 8: 20241015_133555.png
20241015_133555.png
Attachment 9: 20241015_133300.png
20241015_133300.png
Attachment 10: 20241015_133643.png
20241015_133643.png
Attachment 11: 20241015_134202.png
20241015_134202.png
Attachment 12: 20241015_135353.png
20241015_135353.png
  459   Wed Oct 16 13:58:59 2024 Luis MartinUpdateVACRGA Scan

The following figure displays data acquired on 10/09, and it shows that we are no longer below the cleanliness standard. Also, the system's pressure went up to 1.9x10-8 Torr (approximately 7x10-9 Torr previously). This might be due to a leak somewhere in the system. More tests will be performed later.

Attachment 1: 2024-10-09_PostBake1_ArO.png
2024-10-09_PostBake1_ArO.png
  460   Wed Oct 16 14:13:31 2024 LiuUpdate FROSTI with non uniform absorption scattering sources
Slides
  461   Thu Oct 17 13:24:23 2024 ShaneUpdateCDSTiming Chassis issue identified

[Ma, Luis, Shane]

Working theory for the timing chassis issues had been that the 1A breaker was tripping and causing the failure of the Valon 5015 and 3010 to output the timing signal correctly. We just tried bypassing the breaker, running 6 V on the benchtop power supply (set the current limit to 1.5A), with the 5010 generating the sine wave to pass to the 3010. All worked correctly, and there were no issues. Square wave outputted by the 3010 was exactly as desired (image attached) at the correct frequency, and this confirms the issue was the breaker, not the valon 5015. Ready to go ahead with ordering a new replacement breaker.

Attachment 1: IMG_6462.jpeg
IMG_6462.jpeg
Attachment 2: IMG_6464.jpeg
IMG_6464.jpeg
  462   Wed Oct 23 11:48:06 2024 Luis MartinUpdateVACLeak Test Results

[Luke, Luis, Mary, Ma]

On 10/22/24 Luke, Ma, Mary and myself ran a leak test, the results are displayed below. The overall pressure of the vacuum was 2.0e-8 and the temperature readings were 26C for the RGA and 25C for the main volume.

Connection Leak rate (torr)
Tee - RGA 9.4e-12 (very low)
Tee - Cal leak 1.58e-11 (very low)
Tee - ZLR (2.75"-4.5") 7.32e-12 (very low)
ZLR (2.75"-4.5") - Reducing Cross 6.9e-11   (low)
Cross - Elbow 2.34e-11 (very low)
Elbow - Pressure sensor 1.96e-11 (very low)
Cross - Turbo pump (small) 1.91e-9   (lowish)
Cross - Gate valve 1.66e-10 (very low)
Gate valve - Port 7.41e-10   (low)
Port - ZLR (6.0"-8") 2.93e-10   (low)
ZLR (6.0"-8") - Turbo pump (large) 6.15e-11 (very low)
Port - Pressure sensor 2.0e-11 (very low)
Port - Up to air valve 1.42e-11 (very low)
Port - Blank 1.27e-11 (very low)
Port - Feed through port 4.59e-12 (very low)
Lid - Curtain side 3.09e-11 (very low)
Lid - Wall side 4.26e-11 (very low)

 

 

  463   Wed Oct 23 12:08:36 2024 Luis MartinUpdateVACRGA Scan

[Luke, Luis, Mary, Ma]

On 10/22/24 Luke, Ma, Mary and myself ran a RGA scan, the results are displayed below. The overall pressure of the vacuum was 2.0e-8 and the temperature readings were 26C for the RGA and 25C for the main volume.

As we can see, the vacuum is passing cleanliness standards again.

Attachment 1: 2024-10-22_PostBake1_ArO.png
2024-10-22_PostBake1_ArO.png
  Draft   Wed Oct 23 12:33:54 2024 Luke Update Zernike calculation update

PowerPoint slides new

PowerPoint slides older

  465   Fri Oct 25 10:56:30 2024 ShaneUpdateCDSTiming Chassis fixed and reinstalled
[Ma, Shane]

We replaced the 1A breaker in the timing chassis today with a 4A one, and tested that all is working well. The chassis successfully outputted the correct signal (image attached). The real time models have also been restarted and the CyMAC diagnostics screen is showing all green flags. Timing chassis has been closed up and reinstalled in the server rack.

Attachment 1: successful_timing.jpeg
successful_timing.jpeg
  466   Tue Oct 29 16:37:35 2024 TylerUpdateElectronicsRed Pitaya OS Update

The Red Pitaya ecosystem has been upgraded to OS 2.00-35, with a key feature being greater freedom in adjusting the sampling frequency for signal analysis. Before, decimation factors could only be applied if they were a power of 2 (i.e 2,4,8,16,...) up to 65536. Now, the factors can be any power of two up to 16, and any whole number greater than 16 up to 65536. Further information can be found here.

  467   Tue Nov 5 09:56:04 2024 Luis MartinUpdateClean & BakeMR Bake

[Luke, Luis]

On Friday, 11/1/24, the MR was unpackaged and cleaned under the flow bench. We noticed an ink stain on one of the corners of the material. After wiping it down with IPA and Vector Alpha wipes, the stain was removed. However, the material showed some wear.

After cleaning, we placed it in the bake station and applied a stainless steel baking protocol. On Tuesday, 11/4/24, the material was removed from the furnace and packaged in a static shielding bag. The MR was wrapped in Vector Alpha wipes.

  468   Tue Nov 5 11:08:40 2024 Luis MartinUpdateVACISO Test

[Luis, Luke, Ma Michael]

The isolation test was conducted on the vacuum system. Every pump was turned off under vacuum, and pressure measurements were taken every minute for 15 minutes. The results are displayed in the sheet linked at the end of this report. The pressure of the main volume dropped very slowly.

The pressure of the RGA Volume dropped in an exponential manner. The test had to be paused at 11 minutes due to concerns about the pressure exceeding the lowest permitted level for the RGA filament.

After the ISO test was performed, we attempted to tighten the bolts of the small turbo pump on the RGA Volume. However, we noticed that the pressure had increased by nearly an order of magnitude, going from 3.27 × 10-9 Torr to 1.45 × 10-8 Torr when both volumes were separated. We conducted a leak test for that particular flange and found a concerning leak of 2.15 × 10-8 Torr, which had previously been 1.9 × 10-9 Torr. We believe the copper seal was damaged during the ISO test.

View the results sheet

  469   Wed Nov 6 13:48:55 2024 LiuUpdateInterferometer SimulationsQN modeling update
Slides
  470   Wed Nov 13 14:03:32 2024 TylerUpdateElectronicsRIN Update
[Tyler]

We've added two low-pass filters in hopes of reducing any potential aliasing that may be introducing additional noise into the power spectra for the RIN measurements. It still looks like the noise levels are too high. Attached below are some recent measurements taken with the FROSTI powered on and off.

Attachment 1: IMG_0463.jpg
IMG_0463.jpg
Attachment 2: CH0_CH1_ASDs.pdf
CH0_CH1_ASDs.pdf
  471   Wed Nov 13 14:06:00 2024 Luke UpdateGeneral 

slides

  473   Thu Nov 14 11:58:05 2024 ShaneUpdateCDSTurbo pump connection troubleshooting
Attempted connection to the TV551 turbo pump through Varian/Agilent's software on spica. Successful connection established, and we are able to read out al the readings associated with the pump (status, temperature, etc) through the software, which is actually pretty extensive and well organized. Was able to stop and restart the pump with no issues. Serial communications seem to be working fine, and the current serial settings (baud rate 9600, serial type RS232) all match what the Iolan was expecting with the previous connection test. Also notable: the code used for the previous (failed) connection test is written using 'Letter protocol', which is the older of the two communications protocols supported by these kinds of pumps. This rules out the pump being too old to accept the newer communication format as the issue, since it's the older format being used anyway. Will continue trouble shooting to determine why previous connection test failed.
  474   Tue Nov 19 17:10:34 2024 Luke UpdateVACLeak check

Chamber temperature: 23C

Chamber Initial Pressure: ~1.8e-8 main, ~3.5e-8 rga

Did another leak test after monday's work to check how the seal was holding up initial leak was 5.5e-9. I then tried to tighten the bolts a bit more the leak rose to 1.9e-8 about a factor of 4 change.

I checked another flange to confirm that I was preforming the test properly. I measured the elbow to pressure sensor to be 2.2e-11 aproximatly what it was earlier in the month (1.9e-11). 

I ran another isolation test. It is still exponetial. Graph attached.

Thoughts:

I belive at this point that it is a knife edge issue when replacing the gasket I checked both flanges and the new gasket. The tp knife edge seemed perfectly fine, the gasket had very minor scratches, and the reducing cross had very small imperfections on its edge. 

We may want to try and use the liquid sealant or get annealed gaskets for 4.5"

Attachment 1: image.png
image.png
Attachment 2: IMG_5116.jpeg
IMG_5116.jpeg
Attachment 3: IMG_5117.jpeg
IMG_5117.jpeg
  476   Wed Nov 20 12:31:24 2024 LuisUpdateVACLeak test RGA Scan after vacuum repairs

[Luke, Luis]

After the gasket replacement performed on Monday (11/18/24) we let the vacuum pump down to UHV pressure for a couple days. Today (11/20/24) we measured the pressure to be 5.30*e^-9 with a temperature of 22C, and we performed a leak test and RGA Scan.

Here are the results:

Connection Leak rate (torr)
Reducing Cross - TP Left 4.5e-9 (lowish)
Reducing Cross - TP Right 6.0e-9 (lowish)

 

 

Attachment 1: 2024-11-20_PostBake1_ArO.png
2024-11-20_PostBake1_ArO.png
  477   Wed Nov 20 12:59:37 2024 TylerUpdateElectronicsRIN Update
I went ahead and compared the noise spectrum of the ADC to those of the photodetectors with the FROSTI on and off. As discussed last meeting, it looks like the measurements with the Red Pitaya (RP) are limited by the ADC noise floor. Another avenue to explore in this measurement could be switching to the cymac ADCs.
Attachment 1: ASD_plots.pdf
ASD_plots.pdf
  10   Wed Aug 17 16:04:30 2022 Phoebe ZylaSummaryLoreTesting the Cartridge Heater and Collecting FLIR Data

We have tested the heater to find emissivity, mounted the heater system to the optical table, and have taken irradiance maps of the heater projected onto the screen.

The heater's emissivity was determined by using a thermocouple in conjunction with the FLIR's temperature calibration. To attach the thermocouple to the heater initially, I used Kapton tape and ran both the wires of the heater and the thermocouple through the heater bridge. This allowed for the heater to rest on an optical post and be observed without anyone directly holding it, but there were some measurement issues. The thermocouple had a very wide range of temperatures it was reading, which may have been due to intermittent contact or a short between the two legs of the thermocouple. To solve this and make the temperature measurements more stable, we pried apart the two ends of the thermocouple (to ensure there was no short) and put tape on either side, leaving the end connection bare. This was then taped to the heater, and the thermocouple was much more stable. We also used a K-type thermocouple that has an adhesive tape on it already, which assisted with the intermittent contact as well. With the thermocouple measuring the temperature of the heater, we could point the FLIR directly at the heater and calibrate the emissivity until the FLIR and the thermocouple agreed. Cassidy's emissivity calculator was also used, as I could input a temperature and observe what the emissivity of an area was based on that temperature. We found the emissivity of the heater to be 0.57.

As a note, when observing the heater with the FLIR, it appeared that there was a hot spot in the center, where the Kapton tape sat. Because the Kapton has a different emissivity than the 304 stainless steel of the heater, the FLIR will read it as having a different temperature than it actually does. When using the FLIR in the future, be sure to ascertain whether there is a temperature difference somewhere or if there may be different emissivities.

Additionally, the first heater that I used was taken to a very high temperature and oxidized. The emissivity of this oxidized heater is not known, but could be good information for knowing how oxidation affects these heaters specifically.

To mount the heater system in front of the screen, I used 1/2'' optical posts and the mount I designed using COMSOL's CAD program. The heater was originally 2.5 inches away from the screen, and has since been moved back by an additional two inches so that we could observe the heater side of the screen with the FLIR. We wanted to see what temperature the heater side of the screen was when irradiated by the heater, and how that compared to the camera side of the screen. When the heater ran at 1.12 W of input power, the heater side of the screen had a max temperature of around 29.7 C, and the camera side of the screen read at about 29.5 C. This means that there is very little thermal loss between the two sides of the screen, and any insulation that the screen's adhesive may have is largely negligible. Additionally, the camera was placed at an angle and undetermined distance for these tests, confirming that the temperature measurements compensate well/don’t depend on changes in angle or distance between the camera and the screen. However, there was spots on the back of the screen that the camera was measuring as hot spots where there shouldn’t have been any. I have included an example below. It would be useful to run a test where the camera is directly on the back of the screen without the heater to characterize the screen and see if the hot spots are physically present on the screen or if this is an artifice of the camera because of something like angle of viewing.

Taking irradiance maps of the screen was straightforward. After checking that the emissivity of the screen is 0.99 by viewing it at room temperature, we monitored the max temperature while slowing increasing the wattage the heater was running at. There is not a large change until the heater is at around 95 C, at which point the screen began to rise in temperature from 27 C to 28 C. We took measurements of this while the heater was 2.5 and 4.5 inches away from the screen. The irradiance map has a very symmetrical and circular shape, but does not have the ring pattern that we expected. There may be a few reasons for this: there could be some conduction between the two sides of the screen that is causing the pattern to spread further, the heater setup may not be as ideal as it was modeled to be, or there could be a different, unknown issue.

TO DO:

- It would be useful to run a test of the camera in multiple different positions to ensure our conclusion that the camera’s measurements don’t depend on angle or distance (or that these factors are well accounted for in the current temperature calculations) is correct.

- Measure the back of the screen straight on to identify bright spots and possible reasons as to their appearance.

- Recalibrate camera to ensure it is still correct after testing in multiple positions.

- Take another irradiance map of the screen at a higher input power, as well as moving the heater close/further away to try and replicate the COMSOL irradiance maps. It would be useful to also redo the COMSOL modeling at lower powers and variable distances.

Pictures included of full table setup, the heater mount, the heater with Kapton tape attaching the thermocouple as well as FLIR's measured irradiance map.

Attachment 1: Screenshot_(74).png
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AcquisitionImage(Aug-15-2022_14_16).jpg
  19   Fri Feb 3 13:04:04 2023 shaneSummaryGeneralclean room particle counts 1/25/23
Clean room count graphs for each zone (as of January 25, 2023) attached
Attachment 1: cleanroomcountsJan25.pdf
cleanroomcountsJan25.pdf
  29   Mon Feb 13 18:57:53 2023 AidenSummaryGeneralClean and Bake batch 2
Cleaned second batch of SS parts with liquinox for 20 min. Then put in oven for 5 steps; 1. Ramp, 100 degC, 15 min 2. Const, 100 degC, 30 min 3. Ramp, 200 degC, 30 min 4. Const, 200 degC, 48 hours 5. Ramp, 25 degC, (off).
  31   Tue Feb 21 17:51:04 2023 AidenSummaryGeneralClean and Bake batch 4
Bagged and Tagged batch 3 parts by placing no more than two part numbers per bag and taped them with kapton tape and labeled them with their name and part number. Then placed them in the clean room on the work bench. Cleaned batch 4 parts with liquinox and placed the into the oven for 5 steps; 1. Ramp to 100 degC in 15 minutes. 2. Dwell at 100 degC for 30 minutes. 3. Ramp to 200 degC in 30 minutes. 4. Dwell at 200 degC for 48 hours. 5. Turn off and cool down to room temperature. To see the specific parts in batch 4 please refer to the Clean and Bake spread sheet on the Richardson lab page: https://docs.google.com/spreadsheets/d/19gnv1q9l64gxnq76KfcXizbqShJfK0ayn2Js1SiAZok/edit#gid=1765414234
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  38   Tue Feb 28 19:37:22 2023 AidenSummaryGeneralClean and Bake batch 5
Bagged and Tagged batch 4 parts by placing no more than two part numbers per bag and taped them with kapton tape and labeled them with their name and part number. Then placed them in the clean room on the work bench. Cleaned batch 5 part (Viton O-Ring) with liquinox and placed the into the oven for 5 steps; 1. Ramp to 100 degC in 15 minutes. 2. Dwell at 100 degC for 30 minutes. 3. Ramp to 180 degC in 30 minutes. 4. Dwell at 180 degC for 48 hours. 5. Turn off and cool down to room temperature. To see the specific parts in batch 5 please refer to the Clean and Bake spread sheet on the Richardson lab page: https://docs.google.com/spreadsheets/d/19gnv1q9l64gxnq76KfcXizbqShJfK0ayn2Js1SiAZok/edit#gid=1765414234 Hand cleaned stainless steel containers and silver coated screws. Designated each container with its contents with the label maker and placed inside the clean room. Should be noted that the fasteners were very clean before the hand cleaning and showed not dirt on the wipes. Added these parts to the clean and bake data base sheet and designated the type of cleaning as "rough cleaning". Gabriella helped with this cleaning and today was her first day in the lab.
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  42   Fri Mar 3 19:13:33 2023 AidenSummaryGeneralClean and Bake Batch 6
Started to clean the dirtiest of the valves. I could not finish but I definitely made good progress on it. The MDC valve is very dirty and there are many places I could not reach with my fingers. I used Acetone and IPA for this first round of cleaning on it. I also was going to bag the viton O-Ring from the previous Batch, however it seems to have broken during the bake and I am leaving it inside the oven for now.
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  47   Wed Mar 8 19:29:00 2023 AidenSummaryGeneralClean and Bake batch 7
Today gave another cleaning to the MDC gate valve. It is still very dirty an will need more cleaning. I also cleaned the other 3 valves and the argon leak. These are also in bags inside the clean room. I cleaned them by hand with IPA wipes and had to specifically give the MDC up to air valve a harder clean with acetone as it was not getting clean with the IPA. This valve still has a ring around the face as shown in the first image. Be very cautious when moving the parts in the large ESD bag, it may be heavy and the parts will move inside.
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  51   Tue Mar 14 18:21:41 2023 AidenSummaryGeneralClean and Bake batch 8
Starting off Peter and I refilled the deionized water barrel. Then Aiden Cleaned and Bake the FROSTI arms and bases in liquinox for 5 minutes. Then placed them in the oven where they will undergo the following steps; 1. Ramp to 100 degC in 15 min. 2. Dwell at 100 degC for 30 min. 3. Ramp to 120 degC in 30 min. 4. Dwell at 120 degC for 48 hours. 5. OFF Also cleaned the 2.75 MDC Gate valve for 20 minutes (10 minutes each side) in liquinox. It looks significantly cleaner in areas I could not reach before. However some areas like the flat bottom threaded holes are still very dirty. I also made sure to dry it thoroughly and wrapped it in UHV foil until I further cleaning is decided.
  52   Fri Mar 17 19:46:39 2023 AidenSummaryGeneralClean and Bake batch 9
Bagged and Tagged the reflector arms and bases and placed them inside the clean room. Total of 2 bags used. Cleaned and Baked parts in batch 9 on the spread sheet and used the following procedure; 1. Ramp to 100 degC in 15 min. 2. Dwell at 100 degC for 30 min. 3. Ramp to 200 degC in 30 min. 4. Dwell at 200 degC for 48 hours. 5. OFF Also soaked the 2.75" CF gate valve in acetone to try and clean the open threads around the part. Then cleaned it in the ultrasonic washer with liquinox for 20 minutes (10 minutes each side). It looks better than it used to but the threads still seem to be the problem and will probably need even further cleaning.
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