ligo-ex ligo-ds
  Richardson Lab Experimental Log, Page 2 of 10  Not logged in ELOG logo
Entry  Wed Apr 12 16:13:19 2023, Cao, Physics, VAC, Vacuum prep and installation VacAssy230412.png
Aiden, Pamella, Peter, Shane, Cao

Today we started vacuum chamber assembly work

  • 10:16 am: Particle count measurement of clean room
  • 10:34 am: Particle counting finished: meets ISO 5 standard
    1. Zone 3 :
      • 0.3 u: 3159
      • 0.5 u: 789
      • 1.0 u: 83
    2. Zone 4 :
      • 0.3 u: 498
      • 0.5 u: 41
      • 1.0 u: 0
  • 10:45 am: Assemble vacuum feedthrough
  • 11:08 am: Finish assembling feedthrough
  • 11:14 am: Assemble inverted magnetron pirani gauge
  • 11:29 am: Finish assembling magnetron gauge
  • 11:31 am: Assemble calibrated Ar Leak
  • 11:47 am: Finish assembling Ar leak
  • 11:49 am: Assemble up to up-to-air valve
  • 11:59 am: Finish assembling up-to-air valve
  • 12:00 pm: Break for Lunch
  • 1:00 pm: Came back from lunch
  • 1:20 pm: Assemble 45 degree elbow [RGA Line]
  • 1:35 pm: Finish assembling 45 degree elbow
  • 1:35 pm: Assemble Reducing nipple [Pump Line]
  • 1:49 pm: Finish assembling Reducing nipple
  • 1:53 pm: Attempt to install gate valve [Pump line] but bolts could not fit to the gap between 2.5" reducing nipple (0.95" length, shortest 5/16 bolt is 1.5" in total length).
    Thickness of of CF flange on reducing nipple is 0.75" inch. Ideally, we want to have 0.2" engagement to the gate valve, thus0.95" + 0.25" head thickness = 1.2" > 0.95" gap.
    We thus most likely will need a replacement for the reducing nipple. We decided we would hold up on installing the rest of the pump line until we have got components to fix this problem

  • 2:05 pm: Assemble gate valve [RGA line]
  • 2:15 pm: Finish assembling gate valve [RGA line]
  • 2:18 pm: Assemble 4-way cross [RGA line]
  • 2:30 pm: Finish assembling 4- way cross [RGA line]
  • 2:37 pm: Assemble manual bellow sealed angle valve [RGA line]
  • 2:43 pm: Finish assembling sealed angle valve [RGA line]
  • 2:45 pm: Assemble inverted magnetron pirani gauge [RGA line]
  • 2:55 pm: Finish assembling magnetron pirani gauge [RGA line]
  • 2:56 pm: Assemble vacuum hose, thin wall [RGA line]
  • 3:04 pm: Finish assembling vacuum hose, thin wall [RGA line]
  • 3:45 pm: Packing up for the the day
  • 4:00 pm: End-of-date particle count measurement
    1. Zone 3
      • 0.3 u: 1080
      • 0.5 u: 124
      • 1.0 u: 83
    2. Zone 4
      • 0.3 u: 540
      • 0.5 u: 83
      • 1.0 u: 83

Entry  Wed Jun 19 18:45:14 2024, Luke, Update, , Vacuum chamber reassembly  image_2024-06-19_182556383.pngimage_2024-06-19_182631737.pngIMG_1710.jpg
[Luke, Aiden, Mohak , Tyler] On Tuesday we had the silver screws for the spherical cube shortened by a quarter of an inch so that they would fit into the gate valve. We then attached the spherical cube to the vacuum chamber. On Wednesday we finished assembling the RGA line and the main turbo pump.
Entry  Sun Sep 1 16:17:40 2024, Luke, Update, VAC, Vacuum chamber leak checking and re-applying heating tape 

[Luke, Luis, Cinthia, Michal, Tyler]

On the 26th Cinthia, Michal, and I took off the insolation on the vacuum chamber and re-routed it to include the new RGA volume. 

The next day Luis and I finished up the last of the flanges to be attached. We attached the Pirani gauge with a conical reducing nipple to the 2.75" port on the vacuum chamber. We then preformed the Helium leak testing, both flanges were quite low the 2.75" flange had a leak of 1.68e-10 torr and the 1.33" flange of 5.5e-12 torr. The leak on the 1.33" flange was so low it was difficult to know how much of it was real and how much was just noise.

Entry  Tue Jun 25 17:19:42 2024, Luke, Update, VAC, Vacuum chamber leak checking  image_2024-06-25_170036021.pngimage_2024-06-25_170057738.pngimage_2024-06-25_170120030.pngimage_2024-06-25_171238788.png
Currently our main leak is in the RGA line. We found this by closing the gate valve from the main volume to see if which side was leaking more. After identifying this we are pumping down the main volume to see how low it can go the third attachment was taken at 4:16 6/25/24. Pumping started around 3:15. We have not been able to find exactly which flange is leaking, but our guess is on the small blanks and where the cube attaches to the gate valve as seen in the second attachment. We will try a few more things and if the leak is not found/fixed we are planning on changing the configuration of the RGA line to remove the spherical cube, which we believe to be the problem. See fourth attachment for rough sketch of initial idea. We have all of the parts required and they are clean and double bagged in 1129. I have not yet made all the measurements to confirm that this design is feasible.
Entry  Wed Jun 26 16:39:34 2024, Luke, Update, VAC, Vacuum chamber leak checking  image_2024-06-26_162539705.pngimage_2024-06-26_162601616.png
On Tuesday I had isolated the main volume and let it pump down over-night. Today, Wednesday, I checked it and it had only gone down by a small amount compared to when I left it on Tuesday. I then proceeded to tighten down the bolts attaching the tubo-pump to the zero-length reducer while it was under vacuum. This caused the pressure to drop down a few orders of magnitude.
Entry  Tue Feb 28 13:53:17 2023, Pamella, Update, General, Vacuum chamber cleaning  EE5E0296-D362-4EA6-B482-85A629D93B46.jpeg4C0AA805-667E-45AD-8704-03389BD63489.jpeg51CE3D1E-F48E-4F57-8450-8F58C27154BB.jpeg58ADE656-52AD-4F0E-88BA-B993F977A519.jpeg
Pamella, Dr. Richardson and Dr.Cao finished checking and cleaning the interior of the chamber, chamber lid, and exterior of the chamber with Vectra Alpha wipes, IPA and in some parts we used acetone . We flip the chamber and put chamber on the table again. A picture of the specific situation is attached below. The next step from here would be to finish the cleaning the floor . The black residues on the side of the table probably is some reaction between the Vinil and the wipes so is not necessary cleaning this part deeply.
Entry  Wed Jun 21 20:25:05 2023, Cao, Infrastructure, VAC, Vacuum chamber bake attempt 1 6x

TL;DR:

We are not yet able to bake the chamber at 150 deg C due to some current limit, most likely caused power supply switching off. Also, smoke was observed at some insulation points, mainly in the small arm sections, This is likely because the insulation does not fit well and the velcro came into direct contact with heat tape. Some Velcro (made from Nylon/ Polyester) has lower melting temperature point (in 90-120 deg C range)

Full version:

20 June 23:

  • Turn off heater (short term testing) Close valves to RGA line and main volume. Pressure (Torr) readout:
    • Gauge 1 (main volume): 3.43E-6
    • Gauge 2 (RGA line): 2.61E-6
    • Gauge 2 (pump line): 3.8E-4
  • Turn off turbo pump, let vacuum line vent
  • Connect high temperature control unit to main power, power up, set setpoints:
    • Temperature setpoint: 150 deg C
    • High temperature setpoint (to switch off) : 175 deg C
    • Hysteresis: 10 dec C
  • change setpoint of PID control unit to 150 dec C, with high alarm set at 165 deg C
  • Connect power output of high temperature control units to PID temperature control units, ensuring both are off
  • Turn off scroll pump
  • Replace Pirani gauge in front of turbo pump with blanks (see image)
  • Pump the vacuum line back down
  • Open up valves and wait until pressure of full system drop back down to 1E-6
  • Install the high temperature controller thermocouples onto the chamber (see images):
    • One thermocouple is installed on the other side of the cross before the turbo pump
    • One thermocouple is installed on the main volume next to the PID controller RTD
  • Attempt to remove electronic box and magnetic shield of full range gauges:
    • Electronic box is easily removed with an Allen key
    • Magnetic shield cannot be removed since the gap between the vacuum flange and the gauge bolt is too short for a spanner to go in. This is mainly due to the bolt washers are in the way (see images)
    • To remove the magnetic shield, the main volume has to be vented and the gauges need to be readjusted.
  • Attempt to power heaters (but only heat to 80 deg C):
  • Leaving the gauges intact, the high temperature controller + PID controller are turned on to test heating the chamber
  • At this point, both of the high temperature controllers are connected to the same power strip (Vacuum chamber end of the table)
  • After heating up to 65-70 deg C range, the powers turned off on both controllers + the lights on one end of the table
  • Upon inspection, the power strip has turned itself off, I don't know what the model of the power strip but we should check its current limit
  • For a quick test, I connect one of the two heater controlling system to the power board on the work desk while leaving the other running off the same power strip: The heaters appeared to be function ok and able to reach 80 deg C, at which point I turned it off and left for the day

21 June 23:

The goals of today was to remove the electronic boxes and magnetic shields on full range gauges to enable high temperature bakeout

  • Upon returning to the lab, the gauges readout of vacuum pressures were:
    • Gauge 1 (main volume): 3.31E-7
    • Gauge 2 (RGA line): 3.40E-7
  • Venting the both main volume and RGA line
  • Remove the two full range gauges from their flanges
  • Electronic boxes and magnetic shields were removed according to the gauge manuals (see images)
  • Mount the gauges (with only its probing volume) back onto their respective flanges, ensuring that the flange washers do not block access to the magnetic shield screws
  • Only remount magnetic shield + electronic box for one gauge (gauge 2: RGA line) for monitoring chamber pressure
  • Turn on scroll pump and let the chamber pump down
  • Rearrange heater controller connections while waiting for pumping down:
    1. Controllers for bottom + pump & RGA line heaters remain the same: connected to power strip on vacuum end of the table
    2. Controllers for lid + upper chamber main volume: connected to power strip on clean&bake end of the table
  • Once the pressure readout by gauge 2 reached 3 Torr, the turbo pump was turned on and left to run for 45 minutes
  • Upon returning to the lab, pressure on gauge 2 read 5E-6 Torr and was still decreasing
  • Disconnect the ethernet cable to gauge 2, remove its electronic box and magnetic shield
  • Turn on heater controller units and let them drive the heaters to get up 150 deg C
  • At 95 degree range, I could see smoke at some locations, mainly the RGA and pump lines where the insulation do not fit properly and the velcros are likely to be overheated
  • Upon reaching 90 degree range (measured by sensors), the powers turned off on both sides of table (including heaters, lights and scroll pump)
    • Turn off both heaters controllers and unplug them from power strip. Attempt to switch the power strip back on but nothing happened
    • It is now not the power strips problem and must be further down the line from outside the tent, most likely the power supply that these strips connected to: What is the power supply model + current limit?
  • The heater controllers left unplugged, I temporarily plugged scroll pump to the desk power strip so it can still run

    Reply  Tue Jun 27 21:47:56 2023, Jon, Infrastructure, VAC, Vacuum chamber bake attempt 1 IMG_0256.pngIMG_0257.pngIMG_0254.png

The electrical overload problem encountered in ELOG 130 has been resolved. The two heater controllers, which draw up to 14.1 A each, overloaded the UPS and tripped one of its circuit breakers, shutting off power to both power strips mounted above the optical table.

I reset the circuit breaker and rerouted the two heater power cables instead to two separate 20 A outlets in the overhead cable tray outside the cleanroom (both on the LP3B 6 circuit). The two high-limit temperature controllers are now permanently positioned, as shown in the photos. For now, the PID controllers have been left sitting at the table level. I am ordering extension cords that will enable us to move those up to the overhead shelf, as well. I ran the heaters in their new configuration for several minutes without issue. Thus we should be able to now proceed with baking the chamber.

For future clarity, I added labels to power strips around the lab indicating which ones are powered by the UPS. To avoid overloading the UPS, only sensitive electronics or devices that could be damaged by a sudden loss of power should be connected to these.

Entry  Fri May 12 20:28:34 2023, Aiden, Cao, Physics, VAC, Vacuum chamber Helium leak test PXL_20230512_211717602.jpgArLeak_230512.png

[Aiden, Cao]

1. Helium leak test

  • 2:00 pm: Uninstall regulator from nitrogen gas tank and move to helium gas tank. Place helium onto cart and move to the rear door of the clean tent. With the tank remaining outside, feed hose through the flexible wall to use in clean tent - See attached image
  • 2:25 pm: Start Helium leak test: At each CF connection, He gas is sprayed while its level is monitored with the RGA in leak detection mode. A constant flow of helium is maintained until the level of helium detected by the RGA plateaus out.
    • All connections show low helium leak detected (< 3e-11 Amp)
    • The connections with highest leak detected are from reducing cross to flex hose and cross to RGA. They are on 2 - 3e-11 Amps. All other connections are less than 8e-12 Amps. We verified tightness of these two connection but they cannot be tighten any further

2. Argon calibrated leak test

After finishing the Helium leak test.
  • We opened the Ar calibrated leak. Upon opening the valve to allow Ar to flow through, we can see a surge in pressure measured by the gauges from 6.7e-7 mbar to 1.2e-6 mbar. This is then drop down and stabilised around 8.9e-7 after 5 minutes.
  • Upon the the equilibrium is reached, we ran RGA scan twice in Analog mode with the following settings:
    • Points Per AMU: 10
    • Start Mass : 1
    • End Mass : 100
    • Focus Voltage: 90 V
    • Channel Electron Multiplier (CEM) : On
    • CEM Voltage: 1060 V
    • Unit: Amps (ion current)
    The settings is saved as rga100amu_scan.rga RGA application file in C:/Users/controls/Documents/Vacuum/VacuumChamber/RGA. The data file is saved in Data folder as ArLeak_230512.txt. This file contains the current values for corresponding AMUs. Using this dataset, we can obtain our chamber outgassing rate.
  • Using RGA_scan_process.py , which is adapted from Mike Zucker's Matlab code E2000071, and the Ar calibrated leak posted in elog 95 we can compute the outgassing rate to be 150.5E-10 Torr l/s . Our outgassing rate is 37.5 times higher than the required (4.00E-10 Torr L/s per E080177)
  • See image attached for the spectrum and the hydrocarbon (HC) tracer masses used to evaluate outgassing
  • All codes and data are stored in Vacuum git repo . I'll qrite up an instruction to use the code and post it on our wiki page.

After finishing with Ar cal leak test, we close Ar valve, disconnect and turn off RGA. The He tank is moved back to the wall mount. The chamber is ready for baking installation

Entry  Thu Oct 12 12:11:10 2023, Aiden, Update, VAC, Vacuum chamber Helium leak test IMG_4689.jpgIMG_4688.jpg
[Aiden, Tyler, Peter, Jon]

Continued tightening bolts on the turbo pump and 6"-8" reducer to reduce the leak. The final leak test values for the turbo pump flange was 3.0 e-9 and the other 6"-8" reducer flange was 4.0 e-9.

We will continue to let it pump down as the screws could not be tightened anymore. Looks like new gaskets will be needed to reduce the leaking on these flanges.

Entry  Fri May 31 19:37:47 2024, Luke, Update, , Vacuum chamber Disassembly  IMG_1681.jpgIMG_1680.jpgIMG_1680.jpgIMG_1681.jpg
[Luke, Aiden, Jon, Michel, Tyler] Work done: On Tuesday (5/28) we removed the RGA line with minimal difficulty. On Wednesday (5/29) we removed the turbo pump, which had a few bolts that we needed to cut. We borrowed a dremel with ceramic blades from the machine shop to help remove some of the bolts. On Thursday we moved the vacuum chamber onto the floor to check and resecure the heating band on the bottom of the vacuum chamber. We then relocated the posts the vacuum chamber rests on closer to the end of the table and reinstalled the chamber. The post’s height was also reduced from 2in to 1in. Current state of vacuum chamber: The vacuum chamber is currently reinstalled in its new position. Some of the parts on the table will be used in the assembly of the turbo pump and RGA lines with the others being able to be moved to storage.
Entry  Fri Jun 28 18:15:16 2024, Luke, Update, VAC, Vacuum chamber  

We will be configuring the RGA line to remove the spherical cube from the system. Currently our plan for the new design is to connect a 4.5" to 2.75" Reducing Cross to the gate valve on the vacuum system. It will be orientated vertically with the turbo pump on top coming off the end will be a 90 deg elbow. On the bottom there will be a 4.5" to 2.75" Zero length reducer attached to that will be a Tee on one side the pressure sensor and the other the RGA. Connected to the elbow will be the calibrated leak. 

The only parts not readily available are the ZLR and the 2.75" gaskets

Part name Count needed Status/comment
2.75" Tee 1 In use in current RGA line
4.5" to 2.75" Reducing Cross 1 Needs to be clean and baked
4.5" to 2.75" Zero length reducer 1 To be purchased  
2.75" 90 deg elbow 1 Clean needs to be removed from another part
5/16 - 24 X 2.00" Bolts and nuts 16

8 in clean room and plenty in storage they will need to be clean and baked. Plenty of nuts in clean room.

1/4 - 28 X 1.25" Bolts and nutplates 24 12 in use in RGA line and 12 in storage that will need to be clean and baked. Sufficient nutplates in clean room
1/4 - 28 X 7/8" Bolts  12 Plenty of bolts in clean room
2.75" Copper Gasket   6 5 gaskets in clean room and none in storage. So some will need to be purchased
4.5" Copper Gasket 2 About 10 in clean room 
Entry  Thu Jun 29 18:27:26 2023, Jon, Cao, Infrastructure, VAC, Vacuum bake attempt 3: success! NewInsulation.pngBypassLineInsulation.jpg
[Jon, Cao]

Summary : We resolved problems with heaters tripping power and were able to proceed with chamber baking

1. Circuit connection adjustment

After yesterday elog 137, today we resolved most of these issues. After Jon contacted Facilities, the LP3B 6 circuit was reset and the cleanroom filter & light panels resumed to work as normal.

Regarding the connection of the heaters. we made the following adjustments:

  • High-temperature controller powering lid + upper volume heater: connect to LP3B 8 circuit (clean room sides, 2 outlets)
  • High-temperature controller powering bottom + lower volume heater : connect to LP3B 4 circuit (workstation side, 2 outlets)

2. Replacement of vacuum nipple insulation

We had also received new insulation pieces from Worbo today to replace the existing insulation with the new ones (see images). These cover the 2 4" tubes (for 6" flanges ) and the 4 1.5" tubes (for 2.75" flanges). The new insulations fit perfectly on these tubes. I also placed all insulation taken off from the last elog back onto the chamber ( these are insulations for the pumps and RGA lines).

3. Baking

We started ramping up chamber temperature at 1:41 pm over the course of two hours:
  • Starting set point: 40 deg C
  • Step increase: 10 deg C up to 80 deg C, 5 deg C from 80 deg to 120 deg C
  • At each step, the temperature readouts show approx. 2.1 deg C overshooting, wait to settle back to approx 1.5 deg C overshoot before increase the set point again
We noticed some smoke emanating from flexible bypass line insulation but none from other locations that were previously smoking . We think this is because the high winding density around the bypass line for such a small volume. Adjustment for next bake: Change the location of PID controller RTD to the bypass line . For now, we remove the insulation around bypass to prevent insulation overheating and encourage convection cooling (see image)

The temperature of the chamber reached as stable 120 deg C without any power issues at 3:45 pm. I waited another 15 minutes to verify its stability and the official baking duration started at 4:00 pm Jun 29 2023. Since we are baking at 120 deg C instead of the standard 150 deg C for Aluminium, the duration for the bake will be over three days until Monday morning, upon which we will slowly ramp down the the temperature.

Entry  Fri Oct 27 15:16:31 2023, Aiden, Update, VAC, Vacuum Leak Test 
Leak tested the worst flanges on the chamber after moving it and after bake 6. The 6 inch flange connected to the 8 inch reducing nipple is now leaking at 1.5 e-9, previously at 4 e-9. The 8 inch flange connected to the turbo pump is now leaking at 1.9 e-9, previously at 3 e-9. This means that the baking most likely improved the seals on these flanges and a hotter bake might fix the leaks for good.
    Reply  Mon Oct 30 08:42:22 2023, Jon, Update, VAC, Vacuum Leak Test IMG_0659.pngIMG_0660.png

By 5:30 pm Friday, the pressure had reached 8.6e-8 torr and was continuing to fall. So it seems we are OK to proceed with permanentizing this configuration (cable routing, heater tape reinstallation).

Quote:
Leak tested the worst flanges on the chamber after moving it and after bake 6. The 6 inch flange connected to the 8 inch reducing nipple is now leaking at 1.5 e-9, previously at 4 e-9. The 8 inch flange connected to the turbo pump is now leaking at 1.9 e-9, previously at 3 e-9. This means that the baking most likely improved the seals on these flanges and a hotter bake might fix the leaks for good.

 

Entry  Fri Jan 27 18:44:31 2023, Julian , Update, General, Vacuum Chanmber Cleaning 
I used the IPA wipes to wipe down the inside of the chamber the best I could. I cleaned the main chamber but not any of the connecting joints. When I finished I did a once over with a fresh wipe and found no residue.
Entry  Mon Jun 3 09:24:48 2024, Aiden, Update, VAC, Vacuum Chamber Rendering VaccumChamberAssembly__Redesign_with_tee.jpgVaccumChamberAssembly__Redesign_with_tee_top.png
Here is a new render of the vacuum chamber that includes the 2.75 tee to place the Argon leak right next to the RGA. The conical reducer under the spherical cube was also replaced with a 4.5 blank. The height from the bottom of the blank to the bottom face of the chamber is 5.45". With the chamber now on 1" standoffs, we will need a support with a height of 6.45".
Entry  Fri Dec 15 14:03:02 2023, Aiden, HowTo, VAC, Vacuum Chamber Opening 
[Aiden]

1. Turn off the RGA filament and disconnect it.

2. Record the pressure and then close the angle valve and gate valve on the RGA line to isolate it from the system.

3. Turn off the backing and turbo pump and let the turbo pump spin to a stop by slowly leaking the chamber. The slower the safer.

4.Slowly open the vents on the chamber and the turbo pump. Making sure not to raise the pressure too fast.

5. Once done venting the chamber, open the lid by removing the bolts and prying the lid open with a long flat head screw driver.

6. Removed previous parts and placed them into clean bags. Place new parts inside of the chamber and group them together close to the center.

7. Place the lid back onto the chamber and tighten the bolts in a circular pattern until tightened all the way with the wrench.

8. Make sure all vents are closed and turn the backing pump back on.

9. The turbo pump can be turned back on when the pressure reaches e-1 torr.

10. Wait until the chamber reaches a pressure of e-6 torr before opening the angle and gate valve on the RGA line. After the RGA line is open and the pressure is still below e-6 torr, the RGA filament can be turned on and a leak test of the lid should be performed.

11. After the leak test shows no leaks, proceed with starting the low temp bake.

Entry  Fri Mar 15 16:58:55 2024, Aiden, Update, VAC, Vacuum Chamber Frosti Testing bake12_240314_Empty_ArC.pngbake12_240314_Empty_ArO.png
[Luke, Luis, Aiden] On Thursday, March 14 - Took preliminary RGA scans of the empty chamber to compare later on. Vented the chamber and placed the FROSTI into the chamber. Plugged in the DB-25 connectors into the feed through port and checked the connection to make sure there were no shorts before closing the chamber and starting the pumps again. On Friday, March 15 - The pressure in the chamber has come down to 7 e-6 torr. It seems to be coming down much slower despite the little time the chamber was left open for. This may be due to the FROSTI being out on the table for so long and a bake may be needed to bring the pressure down to near UHV.
Entry  Sat Feb 11 00:17:27 2023, Julian, Update, General, Vacuum Chamber Cleaning 20230210_181404.jpg20230210_181424.jpg20230210_181541.jpg20230210_181606.jpg
Today I finished wiping down the rest of the vacuum chamber, specifically focusing on the connecting ports and outside surface of the chamber. When I was finished, I test wiped every surface of the chamber and took pictures confirming the current state of cleanliness; Attachment 1 "Wipes for top and bottom of chamber's upper lip." Attachment 2 " Top and bottom of chamber's lower lip." Attachment 3 "Inside and Outside main chamber." Attachment 4 "Inside connecting ports."
Entry  Thu Feb 23 21:12:33 2023, Julian, Update, General, Vacuum Chamber Cleaning ChamberLid_inside.jpgChamberLid_outside.jpgVacuumChamber_inside.jpg
Today I was able to come in and wipe down both sides of the vacuum chamber lid using the regular alcohol wipes and also wipes that were left to dry in the fume hood then saturated with acetone. I managed to get a good amount of the residue off both the inside and outside surfaces of the lid, then did a test wipe of both sides using acetone-soaked wipes; pictures of the wipes are attached below. Once I finished with the lid, I used another acetone wipe to test wipe the inside of the vacuum chamber. The inside is still giving off residue, but very minimally, a photo for this is attached as well.
Entry  Mon Feb 27 17:09:04 2023, Pamella , Update, General, Vacuum Chamber Cleaning Side_of_Table.jpegWipes_from_table.jpeg
Pamella and Julian finished cleaning the interior of the chamber, chamber lid, and the table. We found some black residue on the side of the table but not sure what the issue is. A picture of the specific area of the table that is giving off the black residue is attached below. The next step from here would be to flip the chamber on its side and finish the cleaning the exterior.
Entry  Wed Jul 5 15:46:47 2023, Aiden, Cao, Infrastructure, VAC, Vacuum Chamber Baking Update bake1_230705.png

Cao and Aiden put the RGA back on to the chamber and measured the outgassing rate after the chamber has cooled down from its first bake. The figure attached shows the RGA measurements with the Argon leak open.

Also put the Full Range Gauge #2 [RGA line] back onto the system to measure the pressure and got a reading of 2.78 E-7 Torr. We believe it is actually lower as the chamber temp is still at 28 degC rather than the 24 it was previously measured at. The gauge also may have needed more time to equilibrate.

Entry  Thu Jul 6 16:16:03 2023, Aiden, Summary, VAC, Vacuum Chamber Baking Update 

Pressure Measured Before Removing Gauge 2.31 E-7 Torr.

Went in and turned on the heating tape in increments of 30 degC until 120 degC was reached. I will let it equilibrate over night and then asses whether or not the chamber can be raised to 150 degC without having the flange to the turbo pump reach over 120 degC as it is not recommended for that flange to be any hotter.

If it can safely be raised to 150 degC, then only 2 days of baking is necessary. If 120 degC is the bake temperature, a week will be needed.

Entry  Thu Jul 20 18:03:19 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update bake2_230720.png

Took another set of RGA data after the second bake has cooled down to 27 degC.

Just by visual comparison to the other graphs, the HC levels of the chamber has gone down further. I will soon overlay the data for an easier comparison.

I also reinstalled the full range gauge above the RGA line. It is still adjusting itself downwards so I will have to check again to get an accurate measurement of the pressure.

Entry  Fri Jul 28 13:46:17 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update bake2_230720_ArC.pngbake2_230720_ArO.pngbake2_230728_Closed_Open.pngbake2_230728_Open_Open.png

Took some more data to look at the HC count. Initial data was from leaving the Argon leak closed and then left it open for 15 minutes and then took data for the open scenario. Attached are the graphs for these where attachment 1 is the closed scenario and attachment 2 is the open scenario.

From these graphs it looks like the signal-noise ratio of our calibration line is poor with the ratio between these two being 1.3. This means that the calibrated leak is barely being detected over the background. This should improve with more baking and pumping. I have also now attached overlayed graphs comparing the chamber when the leak is closed versus when it is open. As well as one comparing the chamber right after the bake versus the most recent data both with the leak open.

Entry  Tue Aug 1 12:10:03 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update bake2_230801_ArC.pngbake2_230801_ArO.pngbake2_230801_Closed_Open.png

Dr. Richardson and I took off the insulation on the lid again to add more insulation in-between the heater tape folds in addition to what was added on top of the tape after discovering discoloration. Also cleaned the lid with IPA wipes.

Also took more RGA data, one with the leak closed and one with the leak open. The graphs below this show that the SNR is improving with the ratio now looking to be around 3. The chamber is still too dirty to be commissioned and we will need to be baked again soon.

Plugged the temperature sensor back in after getting another extension cord. Removed the electronics box for the RGA as well as the full range gauge above the RGA line.

Entry  Mon Aug 21 17:13:25 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update bake3_230821_ArC.pngbake3_230821_ArO.png

Came in to take RGA data and found the turbo pump drawing .38 Amps. This was much higher than what it was on Friday. I investigated and found that the breaker had flipped controlling the power strip that the scroll pump was on. The scroll pump was thus not running. I flipped the breaker back and turned the scroll pump back on. I do not know if this will be a reoccurring problem as this has happened before, or if this was due to the storm. Either way the scroll pump is running and the turbo pump is now only drawing .18 Amps at 31 C.

Below are the graphs for the RGA scan that I took before starting bake 4. I have not overlaid them yet so the first one is for Argon leak closed and the second is the Argon leak open. It seems that the chamber had gotten dirtier since the leak and there is still a lot of water left in the chamber. I assume the water will go away after the low temp bake but the HC count may not go down without a longer baker. I also measured the pressure before starting the bake and it was 4.16 e-7 and 3.31 e-7 torr for t he main body volume and RGA volume respectively.

When starting the bake I noticed that the temperature sensor placed on the cross in the RGA volume was reading 40 C hotter that what the PID controller was reading for the lid. I had to remove some of the heater tape from the cross as it was way too hot compared to the lid. After removing the second strip across the cross it is still much hotter than most parts due to it being such a small part compared to the large lid. I hope that after a little bit of equilibration time that the difference between these numbers will go down. Both PID controllers were set to 120 C. The RGA cross was reading 130 C and the Turbo pump cross was reading 76 C.

Entry  Mon Aug 28 14:43:50 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update bake4_230828_ArC.pngbake4_230828_ArO.png
The PID controllers were turned off on Friday and the chamber was left to cool over the weekend. Just took data and it looks like signal to noise ratio is pretty bad again. I do not know if this means we need a hotter bake or if the chamber needs some more time to cool down. I will overlay this data and make sure to take a second set a bit later to compare. Some good news though is that the chamber has reached a pressure below 10e-8 torr with the full range gauge above the RGA line reading 6.85 e-8 torr and still dropping.
Entry  Tue Aug 29 19:09:21 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update bake4_230829_ArO.pngbake4_230829_ArC.png
Here are some more plots with the RGA data take August 29. It seems that more pumping time has led to the HC levels being dramatically reduced compared to only a day ago. The pressure also rises significantly when turning on the RGA filament and it doe not go back down to the pressure before turning it on while the RGA is still running. The pressure after I left was 6.86 e-8 torr.
Entry  Thu Aug 31 12:56:29 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update bake4_230831_ArC.pngbake4_230831_ArO.pngbake4_230829_ArO.png
Took some more RGA data to see if the HC levels have further declined since bake 4 and it seems that it has started to plateau with August 29 160.7 e-10 Torrl/s and August 31 giving 158.4 e-10 Torrl/s. The pressure of the chamber before taking data was 5.1 e-8 Torr. I have attached an overlay of the data from August 29 and August 31. It seems that the extra two days has not noticeably changed the data and another bake will most likely be needed to meet LIGO's HC specifications. The pressure after leaving the RGA off for a bit was 5.9 e-8 torr and it was still slowly decreasing.
Entry  Fri Sep 15 17:33:35 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update bake5_230915_ArC.pngbake5_230915_ArO.png
Took some more RGA data and see that the chamber has gotten much cleaner since monday. Next step would be another bake with some focus around heating the RGA filament more. The pressure in the chamber before testing was 5.32 e-8 torr.
Entry  Thu Oct 19 11:41:04 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update 6x
[Aiden, Tyler, Mohak]

Took some RGA data when we came into the room. The pressure of the chamber was 8.63e-8 Torr before turning on the RGA filament. We saw the usual spike in pressure when the filament was initially turned on. Took some data and saw that the chamber was definitely dirtier since the vacuum upgrade. See figures below.

Put the heater tape back onto the section that was removed. We may need to rearrange the heater tape again as there was not much heater tape to go around the upgraded section. We also tried to get some of the extra insulation around this section and we able to get some on around the 6-8 inch reducer.

We then took off the electronics for the gauges and the RGA, added the new extension cords to the PID controllers, and then started bake 6 which will go to 120 degC and stay that way until most likely Monday. The pressure before starting the bake was 8.28e-8 Torr.

Entry  Thu Oct 26 13:00:45 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update bake6_231026_ArC.pngbake6_231026_ArO.png
Bake 6 was turned off on Monday. Tooke RGA data today and have posted the data below. The pressure of the chamber after taking data was 3.22 e-8 Torr. The chamber HC levels are still not low enough but I feel with more pumping it will go down as the RGA scan was still slowly going down during the data taking.
Entry  Thu Nov 9 13:48:47 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update bake7_231109_ArC.pngbake7_231109_ArO.png
After bake 7 was stopped on Wednesday morning (11,8,2023), I took RGA data of the chamber to compare to a later scan that will be done on Monday to make sure the chamber has reached its lowest pressure. Below are the graphs.
Entry  Wed Nov 15 21:52:33 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update bake7_231115_ArC.pngbake7_231115_ArO.png
Took RGA data before running the degas mode. Made sure to close off the main volume before running the degas. And left the filament on.
Entry  Mon Dec 4 11:19:50 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update bake8_231204_SSFasteners_ArO.pngbake8_231204_SSFasteners_ArC.pngDecember_04_Ar_Open_Stainless_Steel_Fasteners_Analyzed.pngbake8_231204_SSFasteners_ArO.png
[Aiden]

Took some RGA data of the chamber after it has been cooling down. I do not believe that this data accurately shows the HC levels in the chamber as the pressure is still above where it was at before the bake and was still falling. I believe more time is needed to let the pressure fall and for the RGA filament to remain on to return to a point where the data can be trusted.

Entry  Thu Dec 7 12:42:42 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update December_06_Ar_Open_Stainless_Steel_Fasteners_Analyzed.pngbake8_231206_SSFasteners_ArO.png
After leaving the RGA on for a few days the chamber has settled at 2.01 e-8 torr. I also have good news that the chamber looks to be even cleaner as the HC levels are now the lowest they have been being at 26 e-10 Torr l/s.
Entry  Tue Dec 19 15:45:05 2023, Aiden, Update, VAC, Vacuum Chamber Baking Update bake9_231219_Macor_ArO.pngbake9_231219_Macor_ArC.png
Took RGA data for the macor parts inside of the chamber. With the Ar open the HC levels read 30 torrl/s which is around where it was before the bake.
Entry  Mon Feb 26 15:15:39 2024, Aiden, Update, General, Vacuum Chamber Baking Update 
Started Bake 12 on Wednesday Feb. 21 and turned the bake off on Saturday Feb. 24. This was a normal low temp bake with the PID controllers set to 110 degC.
Entry  Sun Dec 17 19:43:18 2023, Aiden, Update, VAC, Vac Heating Update 
[Aiden]

I measured the temperature of the flanges where some of the electronics will go and I found that the RGA flange was at 55C and the two full range gauges were at 65C. I also stopped bake 9 to cool down for measurement.

Entry  Mon Oct 23 07:28:57 2023, Peter, Update, VLC Update, VLC Mode Matching Carney_VLC_Update.pdf
I have attached a pdf with slides of my latest updates.
Entry  Mon Nov 6 11:31:25 2023, Peter, Update, VLC Update, VLC Mode Matching VLC_Update_11_6_23.pdf
See Update Attached
Entry  Mon Nov 13 06:15:45 2023, Peter, Update, VLC Update, VLC Mode Matching VLC_Mode_Matching_3.pdf
Weekly Updates Attached in pdf
Entry  Thu Sep 7 19:24:25 2023, Peter, Update, VLC Update, VLC Launch Chain IMG-3404(1).jpgIMG-3408(1).jpg
The launch optics up to the Faraday Isolator have been added to the breadboard. In the first image, the optics are (from L to R) the stirring mirror, half-wave plate, polarizing cube, 100mm f lens, electro-optical modulator, Faraday isolator, 50mm lens (not part of final design), stirring mirror (not part of final design)
Entry  Mon Oct 9 11:06:17 2023, Peter, Update, VLC Update, VLC Launch Chain IMG-3540.jpgIMG-3538.jpgIMG-3533.jpgIMG-3522.jpg
Implemented the new stage for the EOM. Took power data at different positions in the launch chain. Beam waist: 0.066mm (beam waist is inside EOM). Power before EOM: 0.473mW. Power after EOM: 0.452mW. Power after Faraday Isolator: 0.415mW. Might need to adjust better to configure for clipping losses. Images of setup are attached below.
Entry  Tue Jan 16 10:01:21 2024, Peter, Update, VLC Update, VLC Faraday Isolator and Mode Matching VLC_Mode_Matching_Design_-_Remastered.pdf
Attached is a PDF of my weekly updates.
Entry  Fri Dec 8 11:15:21 2023, Peter, Update, VLC Update, VLC Assembly IMG_4194.jpgIMG_4195.jpgIMG_4197.jpgIMG_4196.jpg
The optics of the visible light cavity have been assembled. The mode matching telescope is folded through the two stirring mirrors at the corners shown in the image below, with the first lens (f=0.2m) before the first stirring mirror, and the second lens (f=0.5m) between the two stirring mirrors. The distance from the cavity to the edge of the table is 14cm. There is still some work to be done on the alignment of the cavity, as the beam does not seem to be completely centered on the two mirrors.
Entry  Mon Apr 15 11:51:03 2024, Peter, Update, VLC Update, VLC VLC_Update_April_15_2024.pdf
An update on the VLC project is attached below:
Entry  Mon May 13 14:53:29 2024, Peter, Update, VLC Update, VLC VLC_Update.pdf
VLC Update WEEK 7 attached below
ELOG V3.1.3-7933898