ligo-ex ligo-ds
  Richardson Lab Experimental Log, Page 9 of 13  Not logged in ELOG logo
New entries since:Wed Dec 31 16:00:00 1969
ID Date Author Type Category Subjectdown
  328   Mon Feb 19 14:17:50 2024 AidenUpdateVACHeater Element RGA Scan
Three days after the completion of Bake 11, the Heater elements RGA scan looks much cleaner. The HC level is back down to 33 e-10 torrl/s with the pressure at 2.13 e-8 torr. I could not take a= scan with the Argon closed as it was left open during the bake and not closed since then.
  506   Fri Jan 31 15:03:09 2025 Xuesi MaUpdate Heater Element Circuit Check

[Ma] Wed 1/29/2025

No short circuit between heater element ✓

No short circuit to ground on any pin ✓

No short circuit between connectors ✓

Heater Number Power Resistor before (Ohm) Power Resistor now (Ohm) RTD Resistor before (Ohm) RTD Resistor now (Ohm)
1 73.6 73.1 81.8 81.3
2 70.4 69.6 82.1 81.6
3 71 70.5 84.5 84
4 71.5 71 80 79.4
5 70.5 70.2 81.7 81.2
6 72 71.6 79.4 78.7
7 69.2 69 78.2 77.5
8 71.1 70.6 84.2 83.6
  609   Mon Jul 14 20:45:20 2025 Luke SummaryCleanroomHEPA filter performance metrics

[Luke, Luis]

We’ve been looking into methods for evaluating the performance of the HEPA filters in the clean room. Measuring flow rate appears to be a promising approach, since the filter manual specifies a recommended minimum of 70 ft/min.

At the moment, we don’t have a flow rate measurement device on hand. We're currently looking into two options:

  • A standard vane-style anemometer, which is more affordable but may lack sensitivity near the minimum required flow rate.
  • A hot-wire anemometer, which offers better resolution and accuracy at lower speeds, though it's more expensive.

In the next few days, either Luis or I will contact Terra Universal to see if they have any measurement solutions that would integrate well with our clean room setup, or if they can recommend best practices for verifying HEPA performance.

  7   Mon Jul 11 14:29:45 2022 JonOmnistructureGeneralHEPA filter installed
Today I unpacked and installed the new HEPA filter for the lab. It is an Omni CleanAir OCA1210 capable of 1200 CFM. This flow rate is sufficient to turn over the air in the room once every 4 minutes, or 14 times per hour. Hopefully this will cut down on our particulate accumulation issues.
  515   Tue Feb 18 10:02:16 2025 Xuesi MaUpdate Group Meeting Slides 2/18/2025

https://docs.google.com/presentation/d/1WiV2VqS0BzXNCK6VYYQ-Ty8xlHnzXatQaFbMf1-0rsY/edit?usp=sharing

  451   Wed Oct 2 10:31:46 2024 Xuesi MaConfiguration Group Meeting Slides 10/2/2024

Group Meeting slides for Non-deterministic Heater Response.

  82   Thu Apr 27 21:43:07 2023 JonPhysicsVACGrounding vacuum system

This afternoon I made up a green 10 AWG grounding cable and connected it to the vacuum system.

One end is tightly connected to the bottom flange of the vacuum chamber (photo 1). It is run along and up the table framing to the top of the cleanroom, where it exits into the overhead cable tray in the same location as the other power cables. It drops down from the top of the server rack all the way to the bottom, where the other end is connected to the lab's electrical ground in the rear of the 240 V UPS (photo 2).

The connections were confirmed to be secure, but continuity testing with an ohmmeter remains to be done to confirm that the chamber and tabletop are indeed grounded.

  84   Fri Apr 28 18:16:57 2023 CaoPhysicsVACGrounding vacuum system

Quote:

This afternoon I made up a green 10 AWG grounding cable and connected it to the vacuum system.

One end is tightly connected to the bottom flange of the vacuum chamber (photo 1). It is run along and up the table framing to the top of the cleanroom, where it exits into the overhead cable tray in the same location as the other power cables. It drops down from the top of the server rack all the way to the bottom, where the other end is connected to the lab's electrical ground in the rear of the 240 V UPS (photo 2).

The connections were confirmed to be secure, but continuity testing with an ohmmeter remains to be done to confirm that the chamber and tabletop are indeed grounded.

 

[Cao]

Continuity Test

Following from Jon's grounding work on the vacuum system, I did a continuity test with the afternoon with a multimeter. The chamber is indeed grounded:
  • Chamber wall to optical table: continuity confirmed, resistance: 0 Ohm
  • Chamber wall to ground point connection on chamber: continuity confirmed, resistance: 0 Ohm
  • Turbo pump to ground point connection on chamber: continuity confirmed, resistance: 0 Ohm
  • Turbo pump to optical table: continuity confirmed, resistance: 0 Ohm
  • Optical table to chassis frame outside cleanroom: continuity confirmed, resistance: 0 Ohm
  • Front of chassis frame to earth point: continuity confirmed, resistance: 0 Ohm

  645   Tue Sep 16 12:18:09 2025 LiuUpdateInterferometer SimulationsGrid search optimization for single-ring FROSTI
Grid search optimization for single-ring FROSTI
  187   Tue Aug 1 16:22:35 2023 CelesteUpdateTCSGraphical Updates to HOM RH Modification, Tuesday 8/1
Slides 20-33 are newly added (data/graphs from parameter sweep feature-1/8th heater unit length varied from 10% of original to 100% of original).
  180   Fri Jul 28 17:45:45 2023 CelesteUpdateTCSGraphical Updates to HOM RH Modification, Friday 7/28
Updated 1/8th Heater simulation modification graphs. Slides 7, 10, 16-19 are new additions.
  173   Thu Jul 27 10:18:43 2023 CelesteUpdateTCSGraphical Updates to HOM RH Modification
Attached are updated graphs of the irradiance distribution from the 1/8th ring heater units (extruded and reduced in length).
  158   Sun Jul 16 15:21:56 2023 PamellaUpdateGeneralGeneral update about some problems in the lab.
[Pamella]
    General information about the lab facility.
    1. Changed sticky floor mats, because close to entrance the cleanroom, both sticky floor had a many died ants on top.
    2. The light on top of the internet cable bridge is burned out.. I just saw this today but I am not sure if was like this before.
    3. The ant bait traps seem very efficient and right now only a few ants are running around in the lab, most are dead in the bait traps, so probably in a day or two we can change those bait traps.
  331   Tue Feb 20 11:31:49 2024 TylerUpdateCleanroomGarment Cabinet Door Replacement
[Luis, Luke, Pooyan, Tyler]

The replacement door for the HEPA garment cabinet arrived last week, and was installed on Thursday. However, it looks like there's a small gap between the door and where the hinge is attached to the cabinet frame. No screws were provided with the replacement door. If we want to perform any adjustments, we have to be very careful; the screws break very easily.

  500   Tue Jan 21 10:12:02 2025 Luke SummaryGeneralFrosti toy model

[Luke, Liu]

Over the winter break I have been working on this desmos toy model of the Frosti. There are still a few rough spots but I belive that it is a good visual representation of a 2D slice of the frosti. 

  646   Tue Sep 16 12:47:29 2025 Xuesi MaUpdateInterferometer SimulationsFrosti actuation impact analysis
Slides
  389   Fri Jun 28 10:43:13 2024 XuejunUpdateCleanroomFrosti
[Xuejun, Tyler]

We moved Frosti into the cleanroom and debugged it to make sure everything was working. One of the DB25 pins broke off at the connector for element 1 so it needed to be recrimped. Element 6 short circuited but fixed with adjustment to the heater power pin position. We connected the power and sensor connectors to the power box and recalibrated the RTD sensors.

  393   Fri Jul 5 13:17:44 2024 LiuUpdateInterferometer SimulationsFour-quadrant FROSTI-like RH for astigmatic thermal actuation for CE optics
In the CE corner layout design and down selection study, interferometer layouts with large incidence angles on some of the curved optics are being considered, such as the folding mirrors in the "long crab". This however generates astigmatic beams upon reflection and results in mode mismatches in coupled cavities that need to be mitigated. Astigmatic thermal actuation for the optics involved is thus essential. One way we are considering is to implement a FROSTI-like barrel RH that delivers different irradiance for the four quadrants. This post summarizes primitive results on the astigmatic thermal actuation for the HR surface by powering the heater elements from one diagonal differently compared to the other.

For this study, we looked at a simple case with an aLIGO-like test mass geometry (R=0.17m, H=0.2m) plus a barrel RH with 0.02m width at 0.03m from the AR surface with FEniCSx. The irradiance profiles are constant inside the width along the longitudinal direction, and zero outside the width. For the baseline non-astigmatic actuation with constant irradiance azimuthally. We have obtained roughly equal quadratic actuations along the x and y directions, as shown in figure. The total delivered power on the entire barrel is normalized to 1 W. The actuation on the curvature per power Delta S/Delta P in this non-astigmatic case thus is 0.835 uD/W.

For the astigmatic case however, the irradiance for the regions from one diagonal is increased by a given amount, compared to the non-astigmatic case, whereas for the other diagonal regions is decreased by the same amount (thus the total power is unchanged at 1 W). The HR deformation when the power is changed by 50%, for instance, is shown in picture, where the deformation along the x direction is larger than the y direction. The deformation in each direction however remains quadratic, with different curvature per powers for the x and y components, as shown in plot. The actuation on the curvature per power for an increasing amount of astigmatism is shown in plot. In terms of Zernike polynomials, the maximum amount of Z22 (astigmatism) for 1 W of total power is 2um while the remaining curvature content (Z20) is 6nm. This is shown in plot.

  556   Mon Apr 21 16:56:42 2025 MichaelUpdateInterferometer SimulationsFixed Observed Squeezing Curve for Toroidal Mirror Case
We've resolved the issue with the observed squeezing curve for the toroidal mirror case showing worse performance at lower frequencies and better performance at higher frequencies compared to the nominal case. This issue was caused by the beam parameter at the squeezer being fixed before changing the radii of curvature of the mirrors. This has been changed to be fixed after changing the mirrors, and we see an improvement in the toroidal mirror case.
  90   Tue May 2 17:03:14 2023 Jon, CaoPhysicsVACFirst pump-down test of vacuum chamber

[Jon, Cao]

1. Re-routing of cables

We re-routed the connections between the turbo pump and its fan to the controller. Instead of going through the side of the server rack, they are now routed along the the cable tray and came down from the top of the server rack.

2. Planning for vacuum assembly re-configuration

While preparing for our first pump-down, we notices that RGA pump line gate valve, at its fully closed position, is higher than the height of the chamber lid. The full range gauge attached to the RGA line, while not that high, can also cause obstruction during removal/ installation of the vacuum lid. The calibrated leak, eventhough is now running within the perimeter of the optical table, it stills introduce weak points that are susceptible to damage if personnel installing chamber lid may lean onto it. Thus we made a few suggested modification to the vacuum chamber assembly:
  • Move the entire RGA arm to the mirrored CF port, where the Up-to-Air valve is at
  • Move the Up-to-Air valve to the calibrated leak port
  • Move the calibrated Ar leak the main chamber full-range gauge port
  • Move the full-range gauge to the RGA line port

3. First test pump-down

  1. With all valves closed, we started scroll pump, pump line quickly got down to 6.08 mbar from atmospheric 1000 mbar (measured by Pirani gauge, channel 3 on controller )
  2. We open Lesker angled valve and let the RGA arm pumped down, Pirani gauge read 6.3 mbar while the full-range guage on RGA line reads 4.9 mbar ( channel 1 on controller )
  3. We open the pump line gate to expose the pump to the main volume, all gaugues readout immediate rise back up 1000 mbar. After 3 minutes, we started to see channel 3 slowly dropped down. A minute later channel 1 and 2 (main body) also dropped down. The slow pressure dropping speed and 6.3 mbar measured earlier got us suspected that there is some large leaks
  4. We proceed to tighten all the ports as the vacuum is pumped down. In particular, we found that large feedthrough port still required a lot of tightening up
  5. As we tighten up all the ports, after 40 minutes, the gauges are now
    • Channel 1 : RGA line full-range gauge: 2.55E-1 mbar
    • Channel 2 : Main chamber full-range gauge: 2.60E-1 mbar
    • Channel 3 : Pump line Pirani gauge: 2.94E-1 mbar
    Compare this to the scroll pump manual , Table 1, page 3, the ultimate pressure of the scroll pump is 2.5E-1 Torr (3.3E-1 mbar), we thus managed to achieve scroll pump ultimate pressure
  6. Turn on turbo pump : Change turbo pump controller from REMOTE to FRONT PANEL mode by pressing both "COUNTERS" and "MEASURE" buttons at the same time, select "MODE=FRONT"
  7. Shorting interlock pin: since we do not have an interlock signal for the controller, use the provided DB-9 connector that has pin 3 and 8 shorted and connect this to the P1 IN connection at the rear of the controller (see attachment 1 )
  8. Press "START" on the controller to start the turbo pump
  9. The pressure readout from the gauges quickly dropped down. After 3 minutes, the Pirani range is maxed out at 0.5E-3 mbar. After 20 minutes, we recorded the following values:
    • Channel 1 : RGA line full-range gauge: 1.50E-5 mbar
    • Channel 2 : Main chamber full-range gauge: 1.89E-5 mbar
    • Channel 3 : Pump line Pirani gauge: 5.0E-4 mbar
    This is Medium vacuum , we want to further reduce this by 2 orders of magnitude. However, we can run RGA test + helium leak test at this pressure
  10. Turn off turbo pump, wait for 10 minutes, turn off scroll pump, open Up-to-Air valve, all pressure gauges indicated pressure returned back to atmospheric pressure

3. To-do actions

  • Run RGA test to get information about contamination status of vacuum
  • Implement suggested changes in section 2
  • Check and modify suspected poor connection: Pirani gauge on pump line. A gap can be seen between connection. There's no good way to tighten it with the screw. Maybe use threaded pin + hex bolt?
  • Controller communications
  554   Tue Apr 15 11:37:17 2025 CynthiaUpdateInterferometer SimulationsFinishing up mirror coating map step
  181   Fri Jul 28 18:03:07 2023 PamellaUpdateFLIRFinal plot - FLIR
[Pamella]
    1. I was able to plot the final result with the data to the heater. I attached below the "3Combined_HighTemp_Gaussian_Plot." in this plot we can see better behavior on the Gaussian compared to the plot in ELOG 169, I was using the same data but with a different approach. On the ELOG 169, we have the center point isolated data and this new plot is the temperature more than 70 C isolated because we have a very good heater temperature distinguish do background. For the all data I got I was using a power current of 0.20A. To get the data I waited for 30 minutes until the heater became stable and after that, I started to take snaps, I took more than one snap for each one different 6 positions on the screen, and We can see the positions on ELOG 167.
    2. Also I attached the calibration plot ("calibration_plot") between the measurements with the FLIR camera and thermocouple and we can see looks good if we compare the final plot.
    3. For better analyses I attached a plot of the calibration line on the Gaussian plot.
    4. To do: I will finish the final report.
  516   Tue Feb 18 10:12:39 2025 TylerUpdateTCSFinal RIN Plot Update

Below is a preview of the final RIN figure that will be included in the FROSTI instrument paper. A quick summary of what is shown below:

The original RIN CSD measurement is shown on the top panel in red. Frequency bins that exhibit external electronics noise (ex. ADC, photodetector noise, etc.) are identified and shaded in gray. These noisy bins are then excluded from the dataset before beginning the next step in the analysis process: rebinning. Here, the resolution of the spectrum can be changed by averaging frequency bins together within a specified interval, with the goal of pushing the measurement curve closer to the A+ requirement shown in the figure. For demonstration below, the spectrum goes from a resolution of ~0.93 Hz to 14.90 Hz.

  460   Wed Oct 16 14:13:31 2024 LiuUpdate FROSTI with non uniform absorption scattering sources
Slides
  649   Tue Sep 30 12:26:15 2025 LiuUpdateInterferometer SimulationsFROSTI optimization for A#
  347   Wed Mar 6 09:57:52 2024 TylerUpdateTCSFROSTI Wiring

Upon finishing the FROSTI assembly last week, we ran into some electrical issues. An electrical short was found between two of the d-sub pins (2 and 8). It appears that the pins were somehow coming into contact with the aluminum surrounding them. This was causing the power supply to trip. The issue was seemingly fixed by adjusting the positioning of the cabling leading out of the reflector. When handling the device in the future, please make sure to keep the wiring as undisturbed as possible. The setup is rather fragile, and moving the cabling around could potentially reintroduce a short like this.

  601   Tue Jul 1 11:04:00 2025 ChristinaUpdateTCSFROSTI Reconstruction II

[Ma, Tyler, Christina]

Finished external reconstruction of the FROSTI by installing all the pins to the 2 DB 25 connectors. To ensure everything was operating correctly, we did electrical testing by testing continuity and by checking each of the heater elements' RTD and power resistance values and comparing them to what was tabulated in January. Additionally, we organized the wires and added the stands.

  600   Fri Jun 27 15:38:22 2025 ChristinaUpdateTCSFROSTI Reconstruction

[Tyler, Ma, Christina, Luke]

We threaded the wiring of the heater elements through the reflective surfaces and were able to attach each piece with the Macor spacers and connect both sides. We used the guide rails and screws to ensure proper alignment. The only necessary step left is to add the additional external screws for the reconstruction.

  492   Wed Dec 18 15:41:56 2024 TylerUpdateTCSFROSTI RIN
[Tyler]

I have begun the (hopefully) final RIN measurements at 3:30 PM today. If you need to go into the cleanroom at any time between now and Sunday (the 22nd), please do not touch the FROSTI, the Red Pitaya, the photodetectors, or any of the wiring.

  352   Sun Mar 24 11:49:27 2024 AidenUpdateGeneralFROSTI RGA Scan
Took RGA data 1 day after the conclusion of Bake 13. Bake 13 ended on Saturday March 23, the RGA data shown was taken on Sunday March 24. The scan shows that the FROSTI is very clean with no outgassing. The HC levels are at 25 e-10. The pressure in the chamber was also a 1.64 e-8 Torr.
  499   Fri Jan 17 13:27:07 2025 TylerUpdateTCSFROSTI Pre-disassembly
[Tyler, Ma, Cece, Jon, Luke, Cynthia, Michael]

On Tuesday, we prepared the FROSTI for disassembly in anticipation of the APS filming that is set to take place in the labs. The FROSTI has been unbolted from the optical table in the cleanroom, with its wires weighted down and the majority of its screws removed to ensure an easy removal of the reflectors during the filming process.

  350   Tue Mar 19 15:22:27 2024 AidenUpdateClean & BakeFROSTI Legs Clean and Bake
[Aiden, Luke]

Cleaned and baked the Cal Tech FROSTI legs and showed Luke the procedure on how to clean parts.

  455   Wed Oct 2 14:49:59 2024 LiuUpdate FROSTI ETM actuation
Proposed FROSTI ETM actuation on the HOM7 resonance. Animation
  501   Wed Jan 22 10:50:08 2025 TylerUpdateTCSFROSTI Disassembly
[Tyler, Ma, Cece, Luis, Shane, Luke, Cynthia, Liu, Jon]

On Tuesday (Jan 21), we took the FROSTI apart in front of a filming crew. It was a success! The footage is going to be used in an APS video detailing the experimental cosmology research conducted in the department.

The FROSTI reflectors, heater elements, and legs were all bagged separately and a currently being stored in the cleanroom. If you need to do any work in there, please be mindful of these parts. The elements are currently on the shelf above the optical table, and the reflectors are placed on the table in the back corner.

  291   Mon Dec 11 16:20:17 2023 JonSummaryTCSFROSTI Assembly Procedure

Below is the procedure we will follow to assemble the FROSTI prototype.

  1. Install SS guide rods and bottom Macor spacers in bottom reflector
  2. Install AlN elements on top of bottom Macor spacers
  3. Install upper Macor spacers on top of AlN elements
  4. Feed unterminated power and RTD leads through slots in upper reflector
  5. Install upper reflector, using guide rods to slowly lower into position
  6. Install vented SS bolts for reflectors; Macor bolts for heater elements
  7. Remove SS guide rods
  8. Bundle power and sensing cable with PEEK cable ties and SS cable mounts
  9. Terminate power and sensing cable bundles with PEEK DB25M connectors
  345   Wed Feb 28 17:49:18 2024 TylerUpdateTCSFROSTI Assembly - Days 2-3
[Aiden, Jon, Luis, Luke, Michael, Tyler]

FROSTI assembly was completed today. The RTD and power wires were terminated at the DB-25 connectors and the legs were put on. It is currently placed in front of the stand-in test mass (~5 cm away). The FLIR has also been moved back to it's nominal position. As of now, it appears there are some shorts within the power cabling. This will be a focus of tomorrow's work.

Quote:
[Jon, Tyler, Luis, Luke, Mohak, Cynthia, Michael, Aiden]

FROSTI assembly began today. After a final set of RGA scans were taken, the vacuum chamber was vented and the reflectors were removed. The chamber was then resealed and pumped down again. 

Today we completed the installation of the Macor hardware and heater elements between the two reflector halves. Tomorrow we will route, bundle, and terminate the power and sensor cables. 

 

  341   Mon Feb 26 21:23:27 2024 JonUpdateTCSFROSTI Assembly - Day 1
[Jon, Tyler, Luis, Luke, Mohak, Cynthia, Michael, Aiden]

FROSTI assembly began today. After a final set of RGA scans were taken, the vacuum chamber was vented and the reflectors were removed. The chamber was then resealed and pumped down again. 

Today we completed the installation of the Macor hardware and heater elements between the two reflector halves. Tomorrow we will route, bundle, and terminate the power and sensor cables. 

  542   Tue Mar 25 12:56:47 2025 TylerUpdateTCSFROSTI Analysis Finalization

Upon final review of the FROSTI analysis included in the (hopefully) soon-to-be submitted instrument paper, I've made some adjustments to the reflectivity analysis that estimates the amount of power delivered to the test mass by the FROSTI. Initially, as detailed in elog 447, the delivered power was approximated to be 12.6 W (later adjusted to 12.9 W), with roughly 18% of this power being reflected by the test mass. After some final adjustments, this value now is closer to 12.0 W, with 10.2 W absorbed (15% power reflection). Below is a table showing the updated values for the FROSTI prototype tests:

Old Value New Value
Delivered Power 12.9 W 12.0 W
Absorbed Power 10.6 W (18% reflectivity) 10.2 W (15% reflectivity)
Measured Peak Temperature Difference 5.39 +/- 0.03 K 5.26 +/- 0.03 K
Model Peak Temperature Difference 5.42 K 5.21 K
Measured Peak OPD 765 +/- 9 nm 771 +/- 7 nm
Model Peak OPD 630 nm 654 nm
  622   Tue Aug 5 12:21:04 2025 LiuUpdateInterferometer SimulationsFROSTI A# optimization
A# multi-ring FROSTI optimization
  664   Thu Nov 20 13:54:34 2025 TylerUpdateTCSFROSTI A# Optimization and Mesh Convergence Analysis
Attached below are slides discussing FROSTI A# Irradiance optimization and mesh convergence analysis for penetration depth.
  118   Mon Jun 12 12:15:10 2023 PamellaUpdateFLIRFLIR- Take data in the closest point.
[Pamella]
  • Used the closest point possible for the reflector in front of the FLIR camera.
  • 11:32 am : Turned on the electronic device (current on) for started taking data.
  • 11:50 am: Started checking the temperature and the parameters.
  • 12:04 pm: Started taking snap after waited for 30 minutes with the current on. Parameters: Current: 0.13A , Volt: 1.8V and Temperature: 51.4 C.
  • Note: This snap is in the most close point possible, after that I should be change the reflector position and also the optical focus distance in the FLIR camera.
  • We can see, in the photo attached below, thought in this closest position the cable connect to reflector is a bit problem to take a good snap also the have issues to keep very uniform triangles (temperature) in the reflector.
  • To do: I'll change the position on the light inside to see if the problem it is in the focal point inside the reflector (mirror).
  112   Wed May 31 16:55:55 2023 PamellaUpdateFLIRFLIR- Focus distance
[Pamella and Tyler]
  • We changed the FLIR Focus Distance for around 0.55 m.
  • Note: The old focus distance was 1.3 m.
  • We tested this new focus distances and looks good. I attached a snap below.
  • Parameters: 0.1 A , 1.5 V and 38.4 C.
  117   Thu Jun 8 14:51:58 2023 PamellaUpdateFLIRFLIR- Distance
[Pamella, Tyler]
  • Today we change the distance between the FLIR camera and reflector (3D-Mask with mirrors and light). Now the distance is 0.2032 m.
  • Note: This distance is just for take a snap most close possible but we need move again for a little far way because in this distance we can't move up and down the reflector for have data to compare.
  106   Wed May 24 14:06:27 2023 PamellaUpdateFLIRFLIR project - Tests
[Pamella]
    Initial tests
  • 10:30 am : Started trying take some test with the new position/configuration between the 3D reflector-mask and the FLIR camera.
  • 10:41 am : Started running the python code and take a snap. Parameters: 0.10 A, 1.4 V.
  • 10:50 am : Started take the snap.It is possible see the triangles, this is a good thing. Negative thing: The middle/center point for the light maybe would be some problems for the future measurements. Parameters: 0.10A, 1.4 V and 41 C.
  • 11:00 am : Started working to better align the entire structure. And double-check the distance between the 3D reflector-mask and the FLIR camera, following the instructions in Cassidy's Final FLIR Project Report.
  • 11:10 am : Difficult point: I tried to attach the complete FLIR camera to the table, but I had a problem to secure the four screws to the table, the distance is not completely compatible with the table stand. Yesterday I just put two screws in the diagonal position, it works fine, but it's not the correct position to work.
  • 12:00 am : Note: Two triangles take more long time to come back a not (low) irradiation position (east and south point).
  • 2:00 pm : Started running the python code again.
  • Parameters: 0.13 A 1.8 V.
  • 2:30 pm: Started take snap. Parameters: 0.13 A, 1.8 V and 49.1 C
  • 3:00 pm: Note: This time every triangles was able to come back a low irradiation position.
  113   Thu Jun 1 14:41:36 2023 PamellaUpdateFLIRFLIR project - Test without the black wall.
[Pamella]
    Test without the black wall.
      General test:.
  • 11:15 am : Started running the code. Parameters: 0.11 A, 1.9V and focus distance around 0.55m.
  • 11:28 am : Started snapping the screen. Parameters: 0.12 A, 1.8V and 44.1 C .
  • First trying:
  • 01:18 pm : Started testing and collection data. Parameters: 0.09 A, 1.4V. Reference position: (0,0).
  • 01:28 pm : Started snapping the screen. Parameters: 0.10 A, 1.5V and 37.9 C. Reference position: (0,0).
  • Second trying:
  • 01:34 pm : Started testing and collection data. Parameters: 0.08 A, 1.4V. Reference position: (0,-0.10).
  • 01:44 pm : Started snapping the screen. Parameters: 0.09 A, 1.7V and 35.8 C. Reference position: (0,-0.10).
  • Third trying:
  • 01:50 pm : Started testing and collection data. Parameters: 0.08 A, 1.3V. Reference position: (0,-0.05).
  • 02:00 pm : Started snapping the screen. Parameters: 0.09 A, 1.4V and 35.4 C. Reference position: (0,-0.05).
  • Fourth trying:
  • 02:04 pm : Started testing and collection data. Parameters: 0.09 A, 1.3V. Reference position: (0,0.05).
  • 02:14 pm : Started snapping the screen. Parameters: 0.11 A, 1.6V and 41.7 C. Reference position: (0,0.05).
    Note: So today i tried collecting data for every possible position in Y (height) way for starting analyses and compares the triangles shapes. I realize maybe we get a problem because i keep the same time in every try but the final temperature and the parameters change every time, so i will try do a better system to keep the parameters equal, maybe i can wait the reflector be back to a normal temperature after every test or keep the system on all the time and just change the reflector position. I pretty sure this was the problem.
  114   Fri Jun 2 14:28:40 2023 PamellaUpdateFLIRFLIR project - Test without the black wall.
[Pamella]
    Test without the black wall.
    Note: So today i collected data for some positions in axis Y (height) for starting analyses and compares the triangles shapes. I tried keep the same parameters every time.
    First position:
  • 01:20 pm : Started testing and collection data. Parameters: 0.10 A, 1.6V. Reference position: (0,0.05).
  • 01:30 pm : Started snapping the screen. Parameters: 0.10 A, 1.6V and 37.7 C. Reference position: (0,0.05).
  • Second position:
  • 01:34 pm : Started testing and collection data. Parameters: 0.10 A, 1.6V Reference position: (0,0).
  • 01:44 pm : Started snapping the screen. Parameters: 0.10 A, 1.6V and 40.6 C. Reference position: (0,0).
  • Third position:
  • 01:50 pm : Started testing and collection data. Parameters: 0.10 A, 1.6V. Reference position: (0,-0.05).
  • 02:00 pm : Started snapping the screen. Parameters: 0.10 A, 1.6V and 39.1C. Reference position: (0,-0.05).
  • Fourth position:
  • 02:03 pm : Started testing and collection data. Parameters: 0.10 A, 1.6V. Reference position: (0,-0.10).
  • 02:13 pm : Started snapping the screen. Parameters: 0.10 A, 1.6V and 39.6 C. Reference position: (0,-0.10).
  105   Tue May 23 16:52:56 2023 PamellaUpdateFLIRFLIR project - Reinstalling the mask and Reconfiguration FLIR position.
[Pamella]
    Reinstalling the mask and Reconfiguration FLIR position.
  • Today i change the aluminum foil inside the 3D mask. After some tries i was able to have a better shape for the triangles.
  • I reinstalled the connections (the light with the thermometer point). Also i checked for the focal point inside the reflector, looks fine.
  • I did a reconfiguration for the initial tests, without the black wall. I moved the FLIR camera and the Reflector-Mask for other position on the table.
  • To do:
  • Start the test with the power current on.
  • I need figure out a better position for the light cables because in front of the mask isn't a good position for us do measurement.
  149   Thu Jul 6 18:03:19 2023 PamellaUpdateFLIRFLIR project - New configuration
[Pamella]
    Cao suggested using the project without the reflector and mask because in this case we probably got good images around the screen. So I started this yesterday and today I started to get some data to see the stabilization position and check how the parameters fluctuated. I was looking and taking snaps for an hour and a half. I'll repeat this one more time to make sure we have enough data to do analysis.
    To do: The next step is to start collecting data by moving the camera FLIR and covering all six positions on the screen (2x3). Also Aiden is on hand to help and is going to make a new 3D print bridge to have good heater support.
    I attached a image for the new configuration below and a snap data.
  104   Mon May 22 17:08:50 2023 PamellaUpdateFLIRFLIR project - Installing the mask.
[Pamella]
  • The new mask for the reflector.
  • 1:40 pm: Started reconfiguration on the FLIR camera project. Changed the old bridge for the new mask-bridge.
  • 2:00 pm: Started figure out the best way to cutting the aluminum foil with the new mask. Unfortunately, I had been some problems for cutting the perfect shape triangles with the mask because the size inside the triangle is different (smaller) than cutter/knife, so is not able to do the cut with precious and carefully then maybe I need other tool for this job. Also I tried use the scissor, didn't work. However, just for the initial testing I worked with the not perfect triangles shape.
  • 2:49 pm: Started installing/attaching the light in the mask.
  • 3:21 pm: Finished installing the light in the mask-bridge.
  • 3:22 pm: Started testing the current and voltage in the new mask-bridge for make sure the light cable is working well.
  • 3:25 pm: Started measurement the resistance with multimeter.
  • 3:29 pm: The measurement looks fine. The multimeter show us 14.1 Ω;
  • 3:38 pm: Started putting the reflector( with the mask attached) in front of the black wall.
  • 3:44 pm: Started roll the testing with the python code to observer the behavior with this new mask. Parameters: 0.14 A and 1.9 V.
  • 4:00 pm: Started snapping. Parameters: 0.13 A and 1.9 V. Final Temperature: 42.7 C.
  • 4:02 pm: Started trying again with more current. Parameters: 0.16 A and 2.2 V.
  • 4:36 pm: Started snapping. Parameters: 0.16 A and 2.2 V. Final Temperature: 50.3 C.
  • 4:55 pm: For now, we can't see the triangles in the snap so i need do some changes.
  • To do:
    1. Change the FLIR camera position for the other side on the table.
    2. Start the test without the black wall.
    3. Try a better tool to cut the triangles inside the 3D-mask.
  58   Wed Mar 29 16:00:36 2023 PamellaUpdateCamerasFLIR project
Today Pamella and Tyler started work in the updates for the FLIR project. We trie for the first time cover the mirrors with aluminum foil and run the code with this. We work in figured out how the python codes works with real datas. To do: Understand how get the real datas and how to compere that with the old datas. Starting test with the FLIR and mirrors with aluminum foil in with the power on. Testing the FLIR camera more times with the mirrors covered with aluminum foil.
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