ligo-ex ligo-ds
  Richardson Lab Experimental Log, Page 6 of 10  Not logged in ELOG logo
Entry  Sat Feb 24 08:53:38 2024, Jon, Infrastructure, Computers, Matlab upgraded to 2023b on Chimay 
I upgraded Matlab on chimay to the latest stable release, 2023b. From some quick tests, it appears to be in working order. Let me know of any issues.
Entry  Tue Nov 5 09:56:04 2024, Luis Martin, Update, Clean & Bake, MR Bake 

[Luke, Luis]

On Friday, 11/1/24, the MR was unpackaged and cleaned under the flow bench. We noticed an ink stain on one of the corners of the material. After wiping it down with IPA and Vector Alpha wipes, the stain was removed. However, the material showed some wear.

After cleaning, we placed it in the bake station and applied a stainless steel baking protocol. On Tuesday, 11/4/24, the material was removed from the furnace and packaged in a static shielding bag. The MR was wrapped in Vector Alpha wipes.

Entry  Mon Feb 19 14:40:21 2024, Shane, Update, CDS, MEDM screen for FROSTI temp readouts IMG_6094.jpegIMG_6092.jpeg
Here's the latest draft of the MEDM screen for the FROSTI heating elements' temperature readouts. Note that the MEDM screen isn't actually this grainy, this just happens to be a photo of the lab monitor's screen off a phone.
Entry  Thu Feb 29 17:16:48 2024, Shane, Update, CDS, MEDM screen for FROSTI T/P readouts IMG_6259.jpeg
Here's the latest draft of the MEDM screen for the FROSTI temp and power readouts, now with a button linking to the c1msc file display. Size/color/label are all changeable, if adjustment is needed. Checked in execute mode as well, and it's working correctly. Also noticed that the MEDM file name has been changed to FROSTI.adl, which I'm noting here for future reference. Still in medm_sandbox directory.
Entry  Wed Feb 21 23:15:07 2024, Michael, Update, Interferometer Simulations, Long Shoelaces 1 Layout Created in Gtrace and Fixed Ghosting in Beamsplitter long_shoelaces1_desmos.JPGAR_side_with_reflection.PNGAR_side_without_reflection.PNG
I have created the long shoelaces 1 layout for cosmic explorer using gtrace, a slight modification from the shoelaces 1 layout design. I also modified the simulation code slightly to remove ghosting effects in the beamsplitter. Originally the python code specified that the HR and AR sides of the beamsplitter both have the same transmission/reflection. I modified this to the ideal case of: Refl_AR = 0, Trans_AR = 1. I have attached two images below to show the before and after effect of this modification.
Entry  Tue Feb 6 22:40:25 2024, Michael, Update, Scripts/Programs, Long Crab 1 Design Created In Gtrace Long_Crab1.pnglong_crab_1_desmos.PNG
Worked on and completed the python code for the simulation of the Long Crab 1 layout for Cosmic Explorer basing off of Pooyan's original work with the Crab 1 layout. From here I'll look into creating the shoelaces layouts.
Entry  Wed Nov 20 12:31:24 2024, Luis, Update, VAC, Leak test RGA Scan after vacuum repairs 2024-11-20_PostBake1_ArO.png

[Luke, Luis]

After the gasket replacement performed on Monday (11/18/24) we let the vacuum pump down to UHV pressure for a couple days. Today (11/20/24) we measured the pressure to be 5.30*e^-9 with a temperature of 22C, and we performed a leak test and RGA Scan.

Here are the results:

Connection Leak rate (torr)
Reducing Cross - TP Left 4.5e-9 (lowish)
Reducing Cross - TP Right 6.0e-9 (lowish)

 

 

Entry  Tue Nov 19 17:10:34 2024, Luke , Update, VAC, Leak check image.pngIMG_5116.jpegIMG_5117.jpeg

Chamber temperature: 23C

Chamber Initial Pressure: ~1.8e-8 main, ~3.5e-8 rga

Did another leak test after monday's work to check how the seal was holding up initial leak was 5.5e-9. I then tried to tighten the bolts a bit more the leak rose to 1.9e-8 about a factor of 4 change.

I checked another flange to confirm that I was preforming the test properly. I measured the elbow to pressure sensor to be 2.2e-11 aproximatly what it was earlier in the month (1.9e-11). 

I ran another isolation test. It is still exponetial. Graph attached.

Thoughts:

I belive at this point that it is a knife edge issue when replacing the gasket I checked both flanges and the new gasket. The tp knife edge seemed perfectly fine, the gasket had very minor scratches, and the reducing cross had very small imperfections on its edge. 

We may want to try and use the liquid sealant or get annealed gaskets for 4.5"

Entry  Wed Oct 23 11:48:06 2024, Luis Martin, Update, VAC, Leak Test Results 

[Luke, Luis, Mary, Ma]

On 10/22/24 Luke, Ma, Mary and myself ran a leak test, the results are displayed below. The overall pressure of the vacuum was 2.0e-8 and the temperature readings were 26C for the RGA and 25C for the main volume.

Connection Leak rate (torr)
Tee - RGA 9.4e-12 (very low)
Tee - Cal leak 1.58e-11 (very low)
Tee - ZLR (2.75"-4.5") 7.32e-12 (very low)
ZLR (2.75"-4.5") - Reducing Cross 6.9e-11   (low)
Cross - Elbow 2.34e-11 (very low)
Elbow - Pressure sensor 1.96e-11 (very low)
Cross - Turbo pump (small) 1.91e-9   (lowish)
Cross - Gate valve 1.66e-10 (very low)
Gate valve - Port 7.41e-10   (low)
Port - ZLR (6.0"-8") 2.93e-10   (low)
ZLR (6.0"-8") - Turbo pump (large) 6.15e-11 (very low)
Port - Pressure sensor 2.0e-11 (very low)
Port - Up to air valve 1.42e-11 (very low)
Port - Blank 1.27e-11 (very low)
Port - Feed through port 4.59e-12 (very low)
Lid - Curtain side 3.09e-11 (very low)
Lid - Wall side 4.26e-11 (very low)

 

 

Entry  Mon Nov 20 20:45:16 2023, Aiden, Update, VAC, Leak Test 

[Aiden, Luis]

Tested every weld and flange to find leaks. Only found that the flange on the turbo pump and reducing nipple was still at 2e-9 torr on the leak. The chamber still rose in pressure when the two gate valves were closed but no noticeable leak could be found on the lid or welds.

Entry  Tue Jun 6 16:15:09 2023, Peter, Update, VLC Update, Launch Optics for Visible Light Cavity IMG-0882.jpgIMG-0883.jpg
I assembled the first few components of the launch optics for the visible light cavity. Below is an image of the current table configuration, and the image is how the cavity will be oriented on the table.
Entry  Fri Feb 23 15:01:48 2024, Shane, Update, CDS, Latest draft of MEDM screen for FROSTI readouts IMG_6128.jpg23.jpg
Here's the latest draft of the MEDM screen for the FrOSTI temp and power readouts. Also, debugged the text readout boxes so they're now correctly reading out the live temperature and power values.
Entry  Tue Apr 4 09:53:37 2023, Peter, Update, VLC Update, Laser intensity/polarization drift measurements initial_Intens_measure_set_up.jpg
The set up for the next round of beam characterization measurements has begun. The beam is initially passing through a half waveplate, is split at a polarizing beam splitter, and then stirring mirrors are used to properly aim the beam into photodiodes (not yet installed). This is the current configuration of the set up.
Entry  Thu Apr 6 10:20:43 2023, Peter, Update, VLC Update, Laser intensity/polarization drift measurements Optical_Setup_4-6-23.jpg
More optical components were added to the optical set up for laser intensity / polarization drift measurements. Both lenses and both PDs were added to the configuration, as seen in the image below. The beam is already well aligned into the center of both of PDs, and focused nicely by the lens. Both PD's take BNC connecting cables, and the Red Pitaya takes SMA connecting cables. Since we are currently without a BNC to SMA cable, and we do not want to cut, strip, and crimp what we have, then measurement process cannot proceed until we get the cables.
Entry  Fri Apr 28 11:21:01 2023, Peter, Update, VLC Update, Laser intensity/polarization drift measurements IMG-0183.jpg
The Digi-key cables have arrived, and I have began implementing them in the intensity drift measurements. There was a slight problem initially in connecting the SMA to BNC cables from the photodiode to the red pitaya, since the red pitaya was way on the other side of the lab. Cao and I connected the red pitaya to a new ethernet cable that extended far enough for the red pitaya to sit comfortably on the breadboard with the optics. Right now the PDAs are not connected to the red pitaya. I have connected them to the oscilloscope in order to read out how much voltage they produce upon incidence of 532nm laser light. This was done in order to make sure that they do not surpass the limit of the red pitaya (+-1V). I have not acquired a value for the readout voltage of the PDAs since I had to go to class. I will gather this preliminary data soon.
Entry  Mon May 22 16:43:28 2023, Peter, Update, VLC Electronics, Laser intensity/polarization drift measurements S-P_Polarization_Diagram.svgPolar_angle_vs_time.pngRel_Intens_vs_time.png
In order to fully analyze the polarization data taken last Thursday, I needed to convert the signal output (which is in volts) to power (units of watts). I used the power meter to accomplish this. Keeping the exact same configuration of PD's and beam splitting, opened the red pitaya's oscilloscope package. I then took the power meter, and held it in front of the PD to measure the amount of Watts at each PD. I then wrote down the corresponding voltage being seen in the red pitaya. I took 5 sets of measurements for each PD to get experimental accuracy. I then used a simple y = mx + b fit to find out the constant m that converts the input wattage into voltage. For the s polarization, the conversion factor is 0.83. For the p polarization, the conversion factor is 1.12. I then used this data to plot polarization angle as a function of time, and the relative intensity drift as a function of time. The plots are shown below. The physical meaning of the polarization angle is shown in the unit circle diagram below, in which P is the total power.
Entry  Wed May 24 14:28:26 2023, Peter, Update, VLC Electronics, Laser intensity/polarization drift measurements Time_Series_Trial_7_16hrs.pngPower_vs_Time_16hrs.pngPolar_angle_vs_time_16hrs.pngRel_Intens_vs_time_16hrs.png
I went in and took polarization drift data for 16 hours. The run started at 6:08pm and finished at 9:15am the next day. The four plots below are the same plots shown for the 2 hour collection and previous trials, except they extend to 16 hours. The only one that is different is the Power vs. Time graph. This is a graph of the actual incoming power of the laser (as opposed to the signal voltage that the PDA's output into the red pitaya). This was done using the calibration factors of the respective PDA's and as we can see, since there is a difference in the calibration factors between detectors, there is a difference in the power that's coupled into S and P polarization.
Entry  Sat Feb 4 17:01:03 2023, Peter, Update, VLC Electronics, Laser Data OmegaX_M2_Fit_3.pngOmegaY_M2_Fit_3.png
Peter and Ryan took laser beam data. Configuration: 100mm focal length lens is ~100mm from lens. 150mm focal length lens is ~200mm from first lens. Beam waist is ~420mm from second lens. Beam waist is very small still. Had to input large amounts of error in data collection. Took width data successively at points near waist and at >= Rayleigh range. Plots are shown below. Key points: Took a while to figure out optimum configuration for lenses to be placed so that an accessible beam waist could be obtained. Beam waist is still very small. May need to do an ABCD calculation to see if there is anything bigger that can be obtained.
Entry  Wed Mar 8 18:35:52 2023, Pamella, Update, , Lab cleaning  
Today Pamella finished cleaning of the cleanroom, starting with the HEPA vacuuming, mopping and clearing all floor with IPA wipes. Also Pamella and Julian finished cleaning of lab floor, starting with the HEPA vacuuming and mopping. Shane and Pamella wiped down every surfaces of the laser table, computer table and the table with the vacuum pieces inside the cleanroom. Shane, Peter, Tayler, Pamella and Julian then wiped down every surface of the laser table outside the cleanroom. We wiped the main tabletop as well as the legs and all parts for the table. We wiped the computer desk, the boxes, the cabinets and every part outside the cleanroom. For now we finished the lab cleaning.
Entry  Tue Apr 11 17:56:15 2023, Pamella, Update, General, Lab cleaning  
Today Pamella and Julian finished cleaning of the cleanroom, starting with the HEPA vacuuming, mopping and clearing all floor with IPA wipes. Also we wiped down some surfaces of the blue table, computer table and the top of chamber.
Entry  Wed Nov 8 17:55:49 2023, Jon, Update, General, Lab Clean-Up Day 1 

[Jon, Tyler, Shane, Peter, Luis]

Today we completed the first phase of lab clean-up. Activities included:

  • CF/KF parts stored under the cleanroom table were removed and transferred to Physics 1129
  • Cleanroom workbench cleared, with all FROSTI hardware collected into one of the large SS bins
  • High surfaces outside the cleanroom (lights, table enclosure frames, rack, cabinets) wiped down with IPA wipes
  • Floor HEPA-vacuumed outside the cleanroom
  • Sticky mats changed throughout the lab

Tomorrow, we will complete turn-over of the cleanroom (HEPA vacuuming of floors, mopping of floors, IPA wiping of softwalls and work surfaces). Shane will post a forthcoming measurement of the cleanroom particulate levels, post-turnover.

Entry  Mon Jul 31 12:39:01 2023, Shane, Update, Electronics, LED cable assemblies installed  IMG_8514.jpegIMG_8516.jpeg
Today I put together the two LED cable assemblies for the CyMAC and mounted them in the anti-aliasing and anti-imaging chassis.
Entry  Tue Jun 27 14:04:42 2023, Sophia A. , Update, Measuring Noise in Interferometer, Interferometer set up and connection to red pitaya IMG_6756.jpgIMG_6754.jpgIMG_6755.jpg
Today we (Sophia and Tyler) constructed the set-up for the electrical noise calculation that I will be conducting this summer. I have included images of the setup below. Our system is effectively a green laser, that feeds into a type of polarizer, then into a beam splitter which sends the laser light down two arms into detectors. We started by connecting the detectors to an oscilloscope to determine whether the signal will exceed 1V, as the red pitaya (our planned data collection device) cannot receive signals with a higher voltage than 1V. We spent most of our time calibrating the oscilloscope and fine-tuning the set-up so that we would have approximately equal voltages in each arm of the interferometer. Once confirming that the output voltage would not meet or exceed 1V, we switched from an oscilloscope to the red pitaya for our measurements. Now that the system is set up, we will be able to run code in the red pitaya interface that will run an FFT on the signal, and then do noise analysis from there.
Entry  Thu Apr 27 16:23:44 2023, Cao, Pamella and Julian, Physics, VAC, Installing vacuum system (cont.) IMG_0139.pngIMG_0136.png
    [Pamella, Cao and Julian, Shane]
  • Particles account
  • 10:37 am: Starting the particles account
    1. Zone 3:
      • 0.3u: 1662
      • 0.5u: 872
      • 1.0u: 415
    2. Zone 4:
      • 0.3u: 831
      • 0.5u: 124
      • 1.0u: 0
  • 11:14 am: Start removal of calibrated leak to install 45 deg elbow
  • 11:21 am: Elbow installed, re-install calibrated leak back on
  • 11:29 am: Finished re-install calibrated leak, start installing gate valve on pump line
  • 11:47 am: Finished installing gate valve, start installing reducing cross onto gate valve
  • 12:02 pm: Finished installing reducing cross, start installing 90 deg elbow to reducing cross
  • 12:17 pm: Finished installing reducing cross, lunch break
  • 01:24 pm: Come back to the lunch break.
  • 01:26 pm: Start installing vacuum hose to elbow.
  • 01:40 pm: Finished installing vacuum hose.
  • 01:43 pm: Start installing turbo pump.
  • 02:00 pm: finished installing turbo pump .
  • 02:10 pm: Start installing standard wall hose from turbo pump to scroll pump
  • 02:21 pm: finished installing hose onto scroll pump, start installing lid. Remove lid from chamber, insert viton O-ring. Place lid back
  • 02:30 pm: Secure lids with screw. Start installing turbo pump controller cable: Pass cable from outside (controller) up the top of clean tent and connect to 8 pin connector on turbo pump
  • 03:00 pm: Installing air cooling unit for turbo pump, found 8 M3 screws for air cooling unit in the C&B cabinet to install the fan bracket onto the back of turbo pump. Fan control cable is routed up to the top of the cleanroom to the controller
  • 03:15 pm: Installing full-range gauge cable to the controller outside cleanroom. Ethernet cables 1 and 2 are used. Cable 1 is used on the RGA line gauge. Cable 2 is connected to the main body gauge. Cable1 and 2 are connected controller's channel 1 and 2 respectively.
  • 04:00 pm: Finish installing gauges cables. Cables are routed up along the frame to the controller sitting outside the cleanroom
  • 04:15 pm: Finished. End-of-date particle count
    1. Zone 3:
      • 0.3u: 3699
      • 0.5u: 1454
      • 1.0u: 872
    2. Zone 4:
      • 0.3u: 1662
      • 0.5u: 706
      • 1.0u: 290
    Entry  Mon May 1 17:10:25 2023, Julian, Cao, Physics, VAC, Installing Pirani gauge and RGA probe onto to vacuum chamber PXL_20230501_225241491.jpgPXL_20230501_235854958.jpgPXL_20230501_234750795.MP.jpg

    [Julian, Cao]

    • 03:00 pm: Particle count
      1. : Zone 3
        • 0.3 um: 498
        • 0.5 um: 124
        • 1 um: 124
      2. : Zone 4
        • 0.3 um: 748
        • 0.5 um: 457
        • 1 um: 374
    • 03:32 pm: Installing Pirani gauge onto pump line
    • 03:51 pm: Finish installing Pirani gauge, start installing RGA probe
    • 04:03 pm: Finish installing PRGA probe, start routing cable from gauge controller to Pirani gauge
    • 04:30 pm: All ethernet cables are routed and connected to gauge controllers
    • 04:48 pm: Power gauge controller up, all gauges are recognised and readout shows atmospheric pressure as expected (1000 mbar)
    • 04:51 pm: End-of-work particle count
      1. : Zone 3
        • 0.3 um: 1413
        • 0.5 um: 872
        • 1 um: 623
      2. : Zone 4
        • 0.3 um: 374
        • 0.5 um: 166
        • 1 um: 166
    We also closed all the valves so we can start testing vacuum pump down of isolated volume tomorrow.

    Entry  Mon Oct 3 17:21:39 2022, Cao, Update, TCS, Inspection of macor parts 7x
    The macor parts arrived and inspected today. These include:
    1. Macor spacer (drawing: LIGO_Redesign_Macor_Spacer_Drawing_v4.pdf attached below), quantities: 40
      • No defects, damages observed
      • Parts are free from grease/ machining fluid
      • Wall thickness of 1 mm appear to provide sufficient stiffness to part
      • Images of parts: Macor_spacer_0.jpg, Macor_spacer_1.jpg
    2. Macor 5-40 UNC screw (drawing: LIGO_Redesign_Macor_Screw_Drawing_v6.pdf attached below), quantities: 20
      • One screw broke, location of break: should edge between head and shaft (see image Macor_screw_5.jpg )
      • All other screws look ok, no damage observed, clean surface overall
      • Images: Macor_screw_0.jpg , Macor_screw_4.jpg
    Entry  Mon Jun 3 14:14:39 2024, Tyler, Update, FLIR, Initial CIT FROSTI Analysis  CIT_FROSTI_Analysis_Group_Meeting-2.pdf
    [Tyler]

    Attached below are the initial results of the CIT FROSTI testing analysis.

    Entry  Tue Feb 13 11:54:45 2024, Tyler, Configuration, FLIR, In-Air Optical Test Configuration In-air_optical_test_sketch.png

    Below is the proposed schematic for FROSTI optical testing, chosen so enough space is allotted for prototype assembly.

    Steps to be taken include:

    1. Reconstruct FLIR staging apparatus
    2. Move test mass stand-in to cleanroom
    3. Mark FLIR camera position on cleanroom optical table at correct distance
    4. Run ethernet cable into cleanroom
    5. Move FLIR aside to allow for more assembly space
    6. Upon assembly completion, reposition FLIR onto optical table again

    Tentative plan is to begin setup early next week.

    Entry  Tue Mar 19 10:55:30 2024, Tyler, Update, FLIR, In-Air Optical Test FroSTI_Thermal_Profile.png
    Below is an image I took using the FLIR just before leaving for the LVK meeting. The profile is roughly what we would expect (annular). Any distortions seen are likely from the screen not being completely parallel to the plane of the FroSTI (i.e. the screen slightly bends in various locations). Next step: In-vacuum test at CIT.
    Entry  Tue Nov 5 11:08:40 2024, Luis Martin, Update, VAC, ISO Test 

    [Luis, Luke, Ma Michael]

    The isolation test was conducted on the vacuum system. Every pump was turned off under vacuum, and pressure measurements were taken every minute for 15 minutes. The results are displayed in the sheet linked at the end of this report. The pressure of the main volume dropped very slowly.

    The pressure of the RGA Volume dropped in an exponential manner. The test had to be paused at 11 minutes due to concerns about the pressure exceeding the lowest permitted level for the RGA filament.

    After the ISO test was performed, we attempted to tighten the bolts of the small turbo pump on the RGA Volume. However, we noticed that the pressure had increased by nearly an order of magnitude, going from 3.27 × 10-9 Torr to 1.45 × 10-8 Torr when both volumes were separated. We conducted a leak test for that particular flange and found a concerning leak of 2.15 × 10-8 Torr, which had previously been 1.9 × 10-9 Torr. We believe the copper seal was damaged during the ISO test.

    View the results sheet

    Entry  Tue Jun 21 18:31:49 2022, Cassidy and Phoebe, Update, Cameras, IR Absorbing Screen and FLIR Camera Setup IMG_6751.pngIMG_1146.pngIMG_6756.png
    Today we set up the IR absorbing screen and the camera on the optical table, as well as tested that the camera was functioning as expected (picking up heat sources beyond the screen).

    Screen Setup

    The screen was set up by clamping it between two rectangular posts on each side. First, two posts were set up with 22 in. between them (thus allowing the screen to span a total distance of up to 24 in. when clamped down). To best stabilize the screen and to allow for it to be "pulled" taut by exploiting the give in the L-bracket, the L-bracket was bolted on the outside of the post, along the same axis as the screen itself.

    On first attempt, the screen was too thin to be fully clamped between the posts. In order to have it fit snugly, sections of heat shrink tubing was used as a shim at the points where the posts were clamped together. The tubing was slid into the track of one optical post at the desired points. In order to accommodate the shim, the two posts had to be held together, ideally clamped, with the screen and shim in place. Then, the post clamps could be slid into the tracks of the post, moved to the optimal location, and tightened down. This required at least three people: two to tighten one side while the third holds up the screen on the other side. The screen was placed ~1/8" from the edge of the posts and flush with the top.

    Camera Stage Setup

    Once the screen was in place, the camera stage was set up by placing the XY-Translational with Rotation stage on four 3" optical posts. Then, the z-axis stage was placed in the center of that, with another 3" optical post on top, which was then topped with the camera. This was set and clamped down ~22.5" from the screen. This was about 1" closer than expected based on our theoretical models.

    Fine Alignment

    We used the visible camera to fine align the screen and to test the setup. Notably, the visible camera is placed below the infrared and thus requires a calibration in order to ensure the two are aligned on the computer image. This can be set by hand using the FLIR proprietary software (FLIR CamWeb) and adjusting the "MSX alignment". The image mode "Thermal MSX" allows both the visible and IR camera to be displayed at once and the difference in their positioning can be seen. We found an offset of ~0.5m to be nearly accurate (note: using this method, although you can get more accurate than this, the displayed value only has one significant figure).

    In order to align the camera, we first used the exposed top edge to judge whether the camera was appropriately centered on the screen. We set the rotation as close as possible to being in line by eye, then adjusted the y-axis until the gap on both corners was a similar size, thus indicating that the rotation and y-position were correctly set. Rotationally, the camera required only a refinement of -1/2 degree. The y-axis is set at 1.25. Then, the camera was pulled as far from the screen as possible using the x-axis to allow the screen to be easily centered using the z-axis. Once the outlined test mass was centered, the x-axis was used to bring the camera close until the screen just barely filled the field of view. The x-axis is at 2.25. The z axis is set to it full dynamic range at 10. Unfortunately, the camera is still slightly too tall for the screen, likely requiring the purchase of a new optical post about 0.5in shorter the current one. This interchange will likely require a new fine alignment after.

    Basic Imaging Tests

    The camera was also focused on the screen based on the manufacturer's printed distance on the camera itself (using 22.5", or 0.572 m). Using the FLIR proprietary software, the camera appears to be in focus in IR (a hand was used as a good focusing tool for this). Additionally, the camera does pick up heat on the other side of the screen. A hand can be lightly seen warming the screen, as can a soldering iron tip. This was a very imprecise visual tool, but does indicate that the camera and screen are working roughly as expected.

    Next Steps

    A new optical post that is ~2.5" tall should be ordered to replace the one under the camera currently. The heating system also needs to be ordered and set up. Currently we are debating between a parabolic reflector with a hole in the back, and one without, as each would require a different mounting mechanism for the cartridge heater.

    Entry  Mon Apr 3 17:04:05 2023, Aiden, Summary, General, IDP Scroll Pump Assembly IMG_4244.jpg
    Aiden installed the isolation valve and the exhaust silencer kits on the IDP-3 Scroll pump. The entire assembly still needs to be wiped down but overall no residue came off when putting on the kits.
    Entry  Sun Apr 10 15:39:49 2022, Rutuja Gurav, HowTo, Computer Scripts/Programs, HowTo: Renew the Let's Encrypt SSL certificate using certbot 

    Port 80 is kept closed by default. This might be causing the certbot auto-renewal cronjob to fail. Therefore we must renew the certificate manually.


    Step 1: Open port 80. (This is needed as the certificate renewal process runs some tests which requires client communication over port 80)


    Step 2: Run the following command


    sudo certbot certonly --force-renew -d richardsonlab.ucr.edu


    Step 3: Confirm the certificate was renewed by running the following command


    sudo certbot certificates

    Entry  Sun May 14 15:50:48 2023, Cao, Infrastructure, Computers, High resolution display of logrus machine 
    [Cao]

    The display resolution of the logrus has been 1064x768 and has been the only option, which is not great. While remote access to logrus using rdesktop allows rendering a virtual display of user's chosen resolution, it is not fast when using graphic-intensive program. NoMachine allows user to take over and control the machine remotely and thus appears as the same machine. However, NoMachine cannot render a virtual display like rdesktop. This has been limiting the resolution of using logrus via NoMachine.

    On Friday, I found that even though we had NVIDIA Quadro P600 graphic card installed, we were not actually using it. The monitor has been connecting to the the integrated VGA display connector. This uses Microsoft Basic Display Adapter which limits the the resolution. Today I got a HDMI to Mini-display cable to connector the monitor to the Nvidia graphic card. Then in Display settings, go to Graphic settings, then enable Hardware-accelerated GPU scheduling. After restarting the machine, the machine recognised the Display 2using the Nvidia Quadro P600. In multiple displays field, selected "Show only on 2" and remove the VGA connection to the monitor. Logrus is now set at Nvidia Qadro P600 native display resolution of 1920x1080. This is now also the display resolution in NoMachine.

    Entry  Fri Sep 6 14:34:52 2024, Luke , Update, VAC, Heating tape work 

    On the 5th I had tried to start baking the vacuum chamber however certain parts of the chamber were getting too hot and causing the controllers to shut off. So I turned them off so that the next day I could rearrange the temperature probes. I then on the 6th set them up so that instead of overshooting the temperature they would be a little low in places.

    After being left over night the cooler parts of the vacuum chamber got much closer to the desired temperature of 120C.

    Here is a table of the temperatures of the sections of the chamber. Note: After these measurements were taken the PID controllers were set to 125C.

    Location   Temperature (C)
    Lid (PID controller 1 emergency shutoff) 108
    Barrel lower (PID controller 1) 120 
    Barrel upper (PID controller 2 emergency shutoff) 118
    RGA volume (PID controller 2) 120

    Here is a table of temperature of the flanges that have electronics.

    Electronics Temperature (C)
    Pressure gauge (Main volume) 79
    Main turbo pump 64
    RGA 51
    Pressure gauge (RGA volume) 55
    Cal leak 47
    Mini turbo pump 50
    Pirani gauge 45 

    Other temperatures of note:

    The optical table was about 38C

    The cleanroom was around 33C (~91F)

    Entry  Wed Jun 14 15:35:36 2023, Pamella, Update, VAC, Heating system installation  heater_equipment_install.jpg
    [Pamella and Cao]
      Heating system installation - Second day.
    • Today we kept installing the equipment for the heating system.
    • First: Started installing the two heating cable around the chamber vacuum, the arms and covered it with aluminum tape.
    • Second: Started installing the insulation stuff around the vacuum chamber and around the connections points (the arms) in the vacuum chamber.
    • Third:Started installing the heater system (electronic device) and tried testing.
      • Note: The around part of the chamber vacuum was difficult to cover, so we spent a little time on. Also one heater system electronic device wasn't working because one fuse is burned so we could not finished this part and we need wait for a new one to replace and working on it.
    Entry  Tue Sep 3 15:52:56 2024, Luke, Update, VAC, Heater tape initilization  

    [Luke, Tyler, Jon]

    On the 3rd we set up the pid controllers for the heater tapes and after putting on the insulation we started heating them up. We first brought it to ~50C and let it stabilize, there was about a 6-7 degree difference between the RGA and the barrel temperature, with the barrel being higher. We then brought it to 60 then 70C it still maintained the slight difference between the RGA and barrel temperatures.

    Here is a table of the temperatures of the flanges connected to electronics as I left it.

    Electronics Temperature (C)
    Pressure gauge (Main volume) 58
    Main turbo pump 45
    RGA 37
    Pressure gauge (RGA volume) 39
    Cal leak 40
    Mini tubo pump 36
    Pirani gauge 37

    Notes: I removed the electronics from the pressure gauge (main volume) because while it was below the required threshold it was still quite high compared to the other flanges.

    Entry  Mon Jun 12 18:52:00 2023, Pamella, Update, General, Heater system parts - Wiped and bagged heater_equipment_wiped.jpg
    [Pamella]
      Cleaning the heater system parts.
    • 04:32 pm: Started wiping the heater system parts.
    • 06:38 pm: Finished wiping the heater and some parts to the system. I wiped, tagged and bagged the heater system, power cables, adapter cables and power connectors. Also I wiped, bagged and tagged the aluminum foil tape.
    • 06:43 pm: I putted all bags inside the cleanroom.
    • To do: I started but I was not able to finished wiping the heating and cords for the heater system so I will finished this parts after.
    • I attached the photos below.
      Entry  Tue Jun 20 17:28:23 2023, Pamella, Update, Electronics, Heater system parts - Wiped  IMG_7696.jpg
      [Pamella]
        Heating system
        Wiping the heater system parts.
      • 04:37 pm: Started wiping the electronic device part for the heater system (HL101 Series Digital Benchtop temperature limit control).
      • 05:19 pm: Finished wiping the parts to the heater system (HL101 Series Digital Benchtop temperature limit control). I wiped the HL101 Series Digital Benchtop temperature limit control and I didn't bagged and tagged because we should install that soon.
      • 05:23 pm: I putted heater electronic device inside the cleanroom without the bag. Also the electronic device is near to the vacuum chamber and the other parts to heater system.
      • I attached the photo below.
      Entry  Tue Jun 13 21:08:46 2023, Pamella, Infrastructure, VAC, Heater system - Installation IMG_7563.jpegIMG_7561.jpeg
      [Pamella, Cao and Jon]
        Heating system installation
      • Today we started installing the equipments for the heating system.
      • First: Started installing the heating cable on the top lid and covered it with aluminum tape.
      • Second: Started installing the insulation cover on top of the chamber lid.
      • Third:Started installing the heating cable from under the vacuum chamber and covered with aluminum tape.
      • Forth: Started installing the insulation cover under the vacuum chamber
      • Note: The under part of the chamber vacuum was very difficult to cover, so we spent a little time on it and we couldn't finish the whole installation today. So tomorrow we should be able to keep doing the installation.
      Entry  Mon Feb 5 14:17:52 2024, Aiden, Update, VAC, Heater Element RGA Scan bake10_240205_Elements_ArO.pngbake10_240205_Elements_ArC.png
      Here are the new RGA scans for the powered Heater elements. The pressure at the time of taking data was 2.88 e-8 torr. The HC levels are at 40 e-10 torrl/s which is not bad but still higher than the lowest we have recorded.
      Entry  Thu Feb 8 17:37:48 2024, Aiden, Update, VAC, Heater Element RGA Scan bake10_240208_Elements_ArO.pngbake10_240208_Elements_ArC.png
      Took more RGA data now that the heaters are powered by 18V. The pressure of the system during the data taking was 3.8 e-8 torr. The RGA scans seem to have gotten worse as well with this power increase.
      Entry  Mon Feb 12 17:35:47 2024, Aiden, Update, VAC, Heater Element RGA Scan bake10_240212_Elements_ArO.pngbake10_240212_Elements_ArC.pngbake10_240212_Elements_300C_ArC.png
      Took more RGA data before and after increasing the heater elements to 300 degC and before heating them up.

      Started Bake 11 as well to hopefully prevent any hydrocarbons from getting captured by the room temperature walls of the chamber. The PID controllers were set to 100C.
      Entry  Mon Feb 19 14:17:50 2024, Aiden, Update, VAC, Heater Element RGA Scan bake11_240219_Elements_ArO.png
      Three days after the completion of Bake 11, the Heater elements RGA scan looks much cleaner. The HC level is back down to 33 e-10 torrl/s with the pressure at 2.13 e-8 torr. I could not take a= scan with the Argon closed as it was left open during the bake and not closed since then.
      Entry  Mon Jul 11 14:29:45 2022, Jon, Omnistructure, General, HEPA filter installed IMG_1530.png
      Today I unpacked and installed the new HEPA filter for the lab. It is an Omni CleanAir OCA1210 capable of 1200 CFM. This flow rate is sufficient to turn over the air in the room once every 4 minutes, or 14 times per hour. Hopefully this will cut down on our particulate accumulation issues.
      Entry  Wed Oct 2 10:31:46 2024, Xuesi Ma, Configuration, , Group Meeting Slides 10/2/2024 Group_Meeting_10_2.pdf

      Group Meeting slides for Non-deterministic Heater Response.

          Reply  Thu Apr 27 21:43:07 2023, Jon, Physics, VAC, Grounding vacuum system IMG_0141.pngIMG_0140.png

      This afternoon I made up a green 10 AWG grounding cable and connected it to the vacuum system.

      One end is tightly connected to the bottom flange of the vacuum chamber (photo 1). It is run along and up the table framing to the top of the cleanroom, where it exits into the overhead cable tray in the same location as the other power cables. It drops down from the top of the server rack all the way to the bottom, where the other end is connected to the lab's electrical ground in the rear of the 240 V UPS (photo 2).

      The connections were confirmed to be secure, but continuity testing with an ohmmeter remains to be done to confirm that the chamber and tabletop are indeed grounded.

          Reply  Fri Apr 28 18:16:57 2023, Cao, Physics, VAC, Grounding vacuum system 

      Quote:

      This afternoon I made up a green 10 AWG grounding cable and connected it to the vacuum system.

      One end is tightly connected to the bottom flange of the vacuum chamber (photo 1). It is run along and up the table framing to the top of the cleanroom, where it exits into the overhead cable tray in the same location as the other power cables. It drops down from the top of the server rack all the way to the bottom, where the other end is connected to the lab's electrical ground in the rear of the 240 V UPS (photo 2).

      The connections were confirmed to be secure, but continuity testing with an ohmmeter remains to be done to confirm that the chamber and tabletop are indeed grounded.

       

      [Cao]

      Continuity Test

      Following from Jon's grounding work on the vacuum system, I did a continuity test with the afternoon with a multimeter. The chamber is indeed grounded:
      • Chamber wall to optical table: continuity confirmed, resistance: 0 Ohm
      • Chamber wall to ground point connection on chamber: continuity confirmed, resistance: 0 Ohm
      • Turbo pump to ground point connection on chamber: continuity confirmed, resistance: 0 Ohm
      • Turbo pump to optical table: continuity confirmed, resistance: 0 Ohm
      • Optical table to chassis frame outside cleanroom: continuity confirmed, resistance: 0 Ohm
      • Front of chassis frame to earth point: continuity confirmed, resistance: 0 Ohm

      Entry  Tue Aug 1 16:22:35 2023, Celeste, Update, TCS, Graphical Updates to HOM RH Modification, Tuesday 8/1 HOM_RH_Simulation_Progress_80123.pdf
      Slides 20-33 are newly added (data/graphs from parameter sweep feature-1/8th heater unit length varied from 10% of original to 100% of original).
      Entry  Fri Jul 28 17:45:45 2023, Celeste, Update, TCS, Graphical Updates to HOM RH Modification, Friday 7/28 HOM_RH_Simulation_Progress.pdf
      Updated 1/8th Heater simulation modification graphs. Slides 7, 10, 16-19 are new additions.
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