ligo-ex ligo-ds
  Richardson Lab Experimental Log, Page 6 of 10  Not logged in ELOG logo
ID Datedown Author Type Category Subject
  220   Tue Sep 5 16:43:19 2023 AidenUpdateGeneralVAC System Heating Update
Checked on bake 5 today after 3 days of equilibrium. The RGA cross is at 106 C and the turbo pump cross is at 74 C. This was reached while the PID controllers were at 140 C. I will now slowly raise the temperature to 150 on the PID controllers and see if the difference in the RGA cross can be reduced.
  219   Fri Sep 1 19:21:19 2023 AidenUpdateVACVAC System Heating Update
Started bake 5 today. This will hopefully be a longer and hotter bake with it lasting 6-7 days at around 150 C. The pressure in the chamber before removing the full range gauge and RGA box was 5.01 e-8 torr. The Argon leak was also left open for this bake to hopefully get rid of particulates on it. I also put the heater tape I removed last time back onto the RGA cross. This made the heating up process take much longer as I had to not increase too much or the cross would heat above 150 C. Hopefully some PID settings in the future will help with this issue. I was able to set the PID controllers to 140 C and after some equilibrium time I should be able to get the temperature up to 150 C. The temperature sensors are reading 150 C and 77 C for the RGA cross and Turbo pump cross respectively. The Turbo pump is drawing the normal .17 Amps at 33 C.
  218   Thu Aug 31 12:56:29 2023 AidenUpdateVACVacuum Chamber Baking Update
Took some more RGA data to see if the HC levels have further declined since bake 4 and it seems that it has started to plateau with August 29 160.7 e-10 Torrl/s and August 31 giving 158.4 e-10 Torrl/s. The pressure of the chamber before taking data was 5.1 e-8 Torr. I have attached an overlay of the data from August 29 and August 31. It seems that the extra two days has not noticeably changed the data and another bake will most likely be needed to meet LIGO's HC specifications. The pressure after leaving the RGA off for a bit was 5.9 e-8 torr and it was still slowly decreasing.
  217   Tue Aug 29 22:07:38 2023 AidenUpdateGeneralElectronic Bench
Dr Richardson is working on mounting more power supplies in the server rack and is using the electronics bench. Be aware to not move anything on the bench itself.
  216   Tue Aug 29 19:09:21 2023 AidenUpdateVACVacuum Chamber Baking Update
Here are some more plots with the RGA data take August 29. It seems that more pumping time has led to the HC levels being dramatically reduced compared to only a day ago. The pressure also rises significantly when turning on the RGA filament and it doe not go back down to the pressure before turning it on while the RGA is still running. The pressure after I left was 6.86 e-8 torr.
  215   Mon Aug 28 14:43:50 2023 AidenUpdateVACVacuum Chamber Baking Update
The PID controllers were turned off on Friday and the chamber was left to cool over the weekend. Just took data and it looks like signal to noise ratio is pretty bad again. I do not know if this means we need a hotter bake or if the chamber needs some more time to cool down. I will overlay this data and make sure to take a second set a bit later to compare. Some good news though is that the chamber has reached a pressure below 10e-8 torr with the full range gauge above the RGA line reading 6.85 e-8 torr and still dropping.
  214   Mon Aug 21 17:13:25 2023 AidenUpdateVACVacuum Chamber Baking Update

Came in to take RGA data and found the turbo pump drawing .38 Amps. This was much higher than what it was on Friday. I investigated and found that the breaker had flipped controlling the power strip that the scroll pump was on. The scroll pump was thus not running. I flipped the breaker back and turned the scroll pump back on. I do not know if this will be a reoccurring problem as this has happened before, or if this was due to the storm. Either way the scroll pump is running and the turbo pump is now only drawing .18 Amps at 31 C.

Below are the graphs for the RGA scan that I took before starting bake 4. I have not overlaid them yet so the first one is for Argon leak closed and the second is the Argon leak open. It seems that the chamber had gotten dirtier since the leak and there is still a lot of water left in the chamber. I assume the water will go away after the low temp bake but the HC count may not go down without a longer baker. I also measured the pressure before starting the bake and it was 4.16 e-7 and 3.31 e-7 torr for t he main body volume and RGA volume respectively.

When starting the bake I noticed that the temperature sensor placed on the cross in the RGA volume was reading 40 C hotter that what the PID controller was reading for the lid. I had to remove some of the heater tape from the cross as it was way too hot compared to the lid. After removing the second strip across the cross it is still much hotter than most parts due to it being such a small part compared to the large lid. I hope that after a little bit of equilibration time that the difference between these numbers will go down. Both PID controllers were set to 120 C. The RGA cross was reading 130 C and the Turbo pump cross was reading 76 C.

  213   Thu Aug 17 15:18:48 2023 AidenUpdateVACVAC Heating System Update
Relocated the PID controllers so that the heating tape could be plugged in. In the picture the left one controls the top half of the chamber along with the RGA line and has its sensor on the lid near a fold. The right one controls the bottom half along with the turbo pump line and the bypass line and has its sensor on the barrel of the chamber. The chamber is almost ready to bake again and just needs to have the full range gauges and RGA electronics box removed.
  212   Thu Aug 17 15:02:44 2023 AidenUpdateVACVAC Heating System Update

Put the heating tape back on and made sure to have 4 coils around the barrel of the chamber. To make this happen I did not put any heater tape on the ports but made sure to place some of the heater no more than 1 inch away from the ports. Also re-placed some of the heating sensors. For the PID controllers there is one sensor placed on the lid and one sensor placed on the barrel. For the temperature alarms one sensor was placed near the flange of the turbo pump and another placed on the cross in the RGA line. Note that all four of these sensors were placed under the heating tape compared to the last few bakes where they were on top.

The insulation was also put back on and now the chamber should be ready for a low temperature bake after some RGA data is taken before for comparison.

  211   Wed Aug 16 17:17:02 2023 Shane, JonUpdateCDSBinary input chassis powering correctly
Binary input chassis passed power-on test, and is lighting up as expected. Binary output chassis also successfully powered on. AA and AI chassis not powering on correctly, need to do some debugging to find the problem.
  210   Wed Aug 16 16:55:40 2023 Shane, JonUpdateCDSexternal power supply cables finished
All four external power supply cables for the CyMAC chassis are now assembled. Using them now to test if chassis power up correctly.
  209   Tue Aug 15 16:10:06 2023 CelesteUpdateTCS8/15/2023 Simulation Progress
  208   Tue Aug 15 16:04:23 2023 AidenUpdateVACVAC Heating System Update

Pulled off the rest of the heater tape along with the aluminum tape left behind. The aluminum tape adhesive left behind a ton of junk on the walls of the chamber. This is probably due to excessive heating. In order to get the adhesive off I sprayed a vector alpha wipe with acetone and wiped down the walls. This took a lot of acetone to get it off.

When removing some of the aluminum tape I noticed small sections that seemed to have been melted to the silicone part of the heater tape and would have been damaging to try and forcefully remove it.

The heater tape is now ready to be put on again but now with the start of the tape placed on the other side so that the PID controllers can be placed on the shelf above the chamber and be seen outside of the curtain.

  207   Tue Aug 15 13:32:37 2023 SophiaUpdateScripts/ProgramsUpdate on Laser Noise Data Collection and Analysis: Dynamic CSD and PSD Plots
I have now fixed all issues that I was having this morning, and have added text boxes which show the peak values of both PSD's and the CSD alongside the graphs. They also update continuously with the graph. This is shown in the top image. The laser was driven at 400Hz, and had 0.5V peak to peak voltage, both of which appear correctly in the below graphs. Now that the code is almost fully working (we will finish debugging the screenshot method later today), our plan tomorrow is to drive the laser and see how the code performs with it. The below graph is from us driving the function generator at 100Hz to test the range. Update: Bottom graph is new version of graphs with better distribution of both graphs.
  206   Tue Aug 15 10:35:00 2023 SophiaUpdateScripts/ProgramsUpdate on Laser Noise Data Collection and Analysis: Dynamic CSD and PSD Plots
I have successfully added a button to my graphics, but it has posed a strange issue with the CSD and PSD values. When I plot my original code, I still see the pretty peaks that I was getting originally, while my new code (as shown in the video and in the last screenshot) is giving me more of a line. In my code that gives the peak values, the CSD values also tend to fluctuate in this new code as well (shown in the first screenshot), before returning to the real value. I think that there is a problem with the averaging and am hoping to solve this issue today with Tyler. This is good progress though!
  205   Fri Aug 11 18:32:00 2023 AidenUpdateVACVAC System Heating Update

[Dr. Richardson, Aiden] Large Update

Removed most of the insulation on the chamber in order to pull back some of the heater tape to get to the flange connecting the bypass line to the valve under the RGA line. Most of the heater tape on the bottom half of the chamber was pulled off and the rest will need to be removed as well in order to place the start of the heater tape on the barrel of the chamber rather than one of the flanges.

Engaged the valve under the RGA line to prevent it from getting more contaminated. Turned off the turbo pump. Turned off the scroll pump. Let the turbo pump sit for a few minutes to let the fans stop. Then leaked the turbo pump volume by turning the knob slowly on top of the turbo. Then proceeded to unscrew the bypass line after done leaking the volume. Replaced the copper gasket and then proceeded to screw it on while maintaining a circular path to ensure equal pressure on the gasket. BEWARE THAT REUSING SILVER PLATED SCREWS HAS A HIGH CHANCE OF STRIPPING THE SCREW AND WILL RESULT IN A LOT OF WORK TO GET THEM OFF. IT IS RECOMMENDED TO USE NEW SILVER SCREWS. HOWEVER WE HAVE NONE LEFT SO DO NOT TRY TO REUSE ANY SCREWS UNTIL WE HAVE SPARES. We were able to use the remaining two spare screws to tighten the flange to a point where it will not tighten anymore.

Then the lid was removed in order to inspect the inside of the chamber and the Viton O-Ring. The chamber had no physical damage and the viton had some visual damage that may correlate to the failure observed during bake 3. Note that some metal chips were found inside of the o-ring groove and needed to be removed. We changed out the o-ring for a new one and placed the old one inside of an anti static bag labeled "Viton O-Ring". Put the lid back on after inspecting for damage and put the bolts on hand tightened. Started to pump down again by turning on the scroll pump first until full range gauge 1 read below 1 torr and then began to turbo pump. The turbo pump was running for 1.5 hours until it plateaued around 3e-4 torr. We then realized the bolts on the lid needed to be tightened more with a wrench. After further tightening the pressure quickly dropped to 6e-6 torr. In the future the bolts should be tightened with a wrench from the begining.

Then proceeded to Helium leak test every weld, flange, and valve. Two of the flanges needed a little more tightening such as the 2 6" flanges. Other than that the only noticeable leak was from the flange just fixed today, however the leak is 10 times less than how it was yesterday and will most likely not hold the chamber back from reaching low 10e-8 torr pressures.

  204   Fri Aug 11 10:57:20 2023 CelesteUpdateTCS8/11/23 Simulation Progress
  203   Thu Aug 10 18:32:39 2023 AidenUpdateVACVAC System Heating Update

[Dr. Richardson, Aiden]

DO NOT TOUCH ANY VALVES ON THE CHAMBER. THERE IS A PRESSURE DIFFERENTIAL BETWEEN THE RGA LINE, TURBO PUMP LINE AND THE MAIN VOLUME. THE TURBO PUMP WILL BE DESTROYED IF OPENED.

Closed the valves to the turbo pump line and RGA line. Turned the turbo pump back on and saw that the pressure in the RGA Line and Turbo pump line was going down so there was no large leak within that line or with the valves as the main body pressure stayed constant. Then raised the pressure of the main body of the chamber as we suspect the viton o-ring has failed and needs to be changed. The bolts to the lid of the chamber were also removed but the lid was left on.

Then performed a helium leak test on the section of the system that was under vacuum. We found two flanges that had small but significant leaks compared to the others in the lines. The flange connecting the full range gauge to the cross and the flange connecting the stainless steel tube to the valve under the cross. These showed large spikes when sprayed with helium and were then tightened to hopefully fix it. After tightening, the flange under the full range gauge was fixed as the bolts were pretty loose and tightening reduced any spike seen on leak test. The other flange on the SS tube could not be fixed with tightening and it still shows signs of helium leaking through. This flange will need to have its gasket changed to fix this leak. Then left the system where it is in the picture for further changes tomorrow August 11. Again, DO NOT TOUCH THE VALVES ON THE RGA LINE AND TURBO PUMP LINE AS THERE IS A PRESSURE DIFFERENTIAL AND IT WILL DESTROY THE TURBO PUMP IF OPENED.

Note: We also found that the pump under the table had flipped the breaker and needed to be turned back on. This may be something to look into.

  202   Thu Aug 10 15:10:12 2023 JonUpdateVACVAC System Heating Update
I shut down the turbo pump since this is evidently a large leak. We CANNOT turn on the RGA for leak checking with the pressure above 1E-5 Torr. I think we will have to manually inspect it. The most likely cause would be that the Viton seal around the lid overheated and failed.

Quote:
Came in to install one of the Full range gauges. Checked the temperature first of the cross and it was reading 30 C. After installing the gauge above the RGA line the controller was reading 2E-1 torr. Installed the other full range gauge to confirm this and it also read that pressure. There may be a leak so I will let it sit for a bit and then perform a Helium leak test.

  201   Thu Aug 10 14:36:00 2023 AidenUpdateVACVAC System Heating Update
Came in to install one of the Full range gauges. Checked the temperature first of the cross and it was reading 30 C. After installing the gauge above the RGA line the controller was reading 2E-1 torr. Installed the other full range gauge to confirm this and it also read that pressure. There may be a leak so I will let it sit for a bit and then perform a Helium leak test.
  200   Thu Aug 10 14:13:38 2023 CelesteUpdateTCS8/10/23, Simulation Graphical Progress
  199   Wed Aug 9 17:35:26 2023 ShaneUpdateCDSBinary output chassis finished
Finished the internal wiring for the binary output chassis today, which completes its assembly. Also secured ribbon cables and chassis lid with their respective screws. Note: one of the spade lugs' internal metal piece is a little loose and had to be reinserted after falling out once. Seemed secure after this, and I checked continuity on everything and it was all good.
  198   Wed Aug 9 11:32:56 2023 JonInfrastructureGeneralNew power cables

I delivered new NEMA 5-15 (120V / 15 A) power cables to the lab for the following items:

  • WS2 (cleanroom) cart - 10ft cable
  • Electronics workbench overhead LED - 10ft cable
  • Both PI heater controller sets - (2) 6ft cables

I installed the new cables on the WS2 cart and the workbench myself, and left the two 6ft cables (as pictured below) for Aiden to install on the PID controllers after the current bake is finished.

  197   Tue Aug 8 17:03:22 2023 Shane, JonUpdateCDSBinary input chassis finished
Finished assembly of the binary input chassis today, including DC on/off switch and LED installation. external cable assemblies still needed, but internal work done.
  196   Tue Aug 8 16:47:11 2023 SophiaUpdateScripts/ProgramsUpdate on Dynamic CSD and PSD Plots
We have fixed our rapid plotting error, and realized that this has not been affecting our data intake! Below is a video of the code progressing, alongside grabbed images of the raw data. The data is now continuous, and performs as we expect. Next, I plan to add a widget which will dynamically show the peak values instead of them just being printed in the terminal after each iteration. (Ignore the red box-- it was from me struggling with a now fixed issue).
  195   Tue Aug 8 15:31:26 2023 AidenUpdateVACVAC Heating System Update

Vacuum Chamber equilibrium temperature for bake 3 are 126 C and 88 C for the chamber wall and turbo pump flange respectively. There were reached with the PID controllers both being set to 150 C.

Also noticed some discoloration around the port insulation. It could be burned from being exposed to the heater tape directly without insulation or it could be that the insulation, which looks much different, is depositing something around the ports.

The turbo pump overheated and the heating tape had to be turned off in order to get the pump back online. It was unusually hot at 52 C. Hottest it got in bake 2 was 38 C.

  194   Mon Aug 7 15:36:18 2023 SophiaUpdateScripts/ProgramsUpdate on Laser Noise Data Collection and Analysis: Dynamic CSD and PSD Plots
Today I was able to fix the red pitaya's plotting problem, and get my code to recognize driving frequencies from the function generator to within a 0.5 Hz estimation. The sinusoidal plots I have included are from sending a 1 Hz signal into the red pitaya to see the signal in real time. This allowed me to see exactly where the system was messing up, and fix from the ground up. Once I had that working, I began to test sending in frequencies in the range that my PSD/CSD code could observe and I was able to identify each driving frequency within 0.5 Hz. My code was able to correctly identify a 500 Hz signal, while other analyzed frequencies in the observable range have fallen lower than the sent in frequency by a less than 0.5 Hz. I believe this issue comes from the strange speed that the red pitaya is still acquiring data, even with my fixing it to now observe a continuous signal.
  193   Mon Aug 7 13:58:46 2023 shaneUpdateCDSinternal power supply cables done for AI chassis
Finished assembling and installing the aLigo chassis internal power supply cables in the anti-imaging chassis today. Tested for continuity and everything looked good. Chassis lid still secured with two temporary screws because I'm not sure what the correct size is.
  192   Fri Aug 4 15:21:33 2023 AidenUpdateVACVAC System Heating Update
Checked on Bake 3 today and the temperature sensors read 126 C and 91 C for the chamber barrel and turbo pump flange respectively. These were reached while the PID controllers were set to 150 C.
  191   Thu Aug 3 18:03:42 2023 Shane, JonUpdateCDSAnti-Aliasing chassis complete
We finished installing the internal power supply cables in the anti-aliasing chassis today, which concludes its assembly. Work on AI, BI, BO chassis still underway.
  190   Thu Aug 3 17:47:51 2023 AidenUpdateVACVAC Heating System Update

Did some further testing to determine if it was within reason to increase the temperature of the chamber. I used a thermometer and pulled back some insulation to test many points on the chamber. Mainly focused on the barrel and the bottom lid of the chamber to see if it was possible to increase the temperature of just the PID controller that is powering the bottom half of the chamber.

Found that the barrel of the chamber seems to be hotter than what the sensor is saying, 125 C. Found many points on the barrel that reached 140 C. I believe this is because the sensor is taped on top of the heater tape rather than in between the aluminum and the heater tape.

Also measured many points on the bottom lid as it has the same configuration the top did before it damaged the insulation. It seemed to be consistently at 150 C but I was able to find a couple points that were hotter around 160 C. These hotter spots were most likely the heater folds. There is not much we can do about this as removing the insulation for fixing would required a very invasive procedure to do it safely.

Then moved to the stainless steel tube that connects the RGA and Turbo pump lines. This tube was around 150 C but many points on it were hotter around 160 C. Before another bake I think some of the tape around the tube may need to be pulled back and relocated to avoid damaging insulation while also providing more heat to the main body of the chamber.

Measured a couple more points on the cross that connects the RGA and the full range gauge and found it to be around 130-140 C which means this section could be hotter as the electronics of the full range gauge can reach 150 C.

Over all I believe that the chamber temperature should not be increased in its current state as the bottom lid is a concern with what happened with the top in the second bake. Some optimizations could be made for a fourth bake however. Moving the temperature sensors to be between the heater tape and chamber. Pulling some of the heater tape from the stainless steel tube and relocating it to the main body of the chamber. Moving the PID temperature sensor on the tube to be on the bottom lid or another hotter spot. These are some changes I would make for a fourth bake but maybe this bake could be the last with how the second bake went.

  189   Thu Aug 3 16:00:25 2023 AidenUpdateVACVAC System Heating Update
Check on the temperature of the bake today to see the equilibrium temperatures. With both of the PID controllers set to 150 C, the temperature sensors for the wall of the chamber and the flange in front of the turbo pump read: 125 C and 90 C respectively. At these temperatures the bake would need to last at least a week unless the temperature were to be increased.
  188   Wed Aug 2 17:02:38 2023 AidenUpdateVACVAC System Heating Update

Moved the temperature sensor on the PID controller to one of the switch backs on the lid.

Also started the next bake with both PID controllers set to 150 degC. When leaving the temperature sensors above the chamber read 119 C and 83 C. These sensors are on the chamber wall and flange in front of the turbo pump respectively.

  187   Tue Aug 1 16:22:35 2023 CelesteUpdateTCSGraphical Updates to HOM RH Modification, Tuesday 8/1
Slides 20-33 are newly added (data/graphs from parameter sweep feature-1/8th heater unit length varied from 10% of original to 100% of original).
  186   Tue Aug 1 15:44:31 2023 SophiaUpdateScripts/ProgramsUpdate on Laser Noise Data Collection and Analysis: Dynamic CSD and PSD Plots
We have identified two problems facing the intensity noise calculations, which we are working to solve. The first of these problems, is that the red pitaya appears to be taking data approximately 4 times faster than we would expect from the decimation rate based on how quickly it runs. To see if this was affecting our data, we plugged the red pitaya into a function generator. We found that my code is able to identify the driving frequency, but consistently gives predictions that are roughly 7% greater than we expect. When we drive at 100 Hz, the plot says the peak is at 107 Hz, when driven at 400 Hz, we see between 422-427 Hz, etc. While this implies that the red pitaya is not taking data at a faster rate than we would expect (if it did we would anticipate a lower than expected frequency, by a factor of roughly 4), it does imply some intrinsic issue with either the red pitaya or with the code. To fix this, I am going to use my code on artificially generated signals and see if we still observe these issues.
  185   Tue Aug 1 12:48:41 2023 AidenUpdateCleanroomPre Filter Change

Changed the pre filter inside of the 3 stage HEPA system next to the soldering station. It was rather dirty and I have attached images with a clean filter on the left and the used one on the right. I reset the pre filter age on the system. I tried to see if I could tell if the HEPA filter was dirty but I could not see it. I did not reset the age of the HEPA or UV stations. They are currently 378 days old.

  184   Tue Aug 1 12:10:03 2023 AidenUpdateVACVacuum Chamber Baking Update

Dr. Richardson and I took off the insulation on the lid again to add more insulation in-between the heater tape folds in addition to what was added on top of the tape after discovering discoloration. Also cleaned the lid with IPA wipes.

Also took more RGA data, one with the leak closed and one with the leak open. The graphs below this show that the SNR is improving with the ratio now looking to be around 3. The chamber is still too dirty to be commissioned and we will need to be baked again soon.

Plugged the temperature sensor back in after getting another extension cord. Removed the electronics box for the RGA as well as the full range gauge above the RGA line.

  183   Mon Jul 31 19:27:30 2023 SophiaUpdateScripts/ProgramsUpdate on Laser Noise Data Collection and Analysis: Dynamic CSD and PSD Plots
An update on the CSD/PSD code: The code is now taking a dynamic average of the points, and that has significantly reduced the noise that we were reading and the issues I was having with the lines in the plots. The graph for the CSD is still putting up a fight though, and amassing many lines that do not appear when just scatter plotted. I plan to fix that tomorrow, alongside inserting my own generated signal into the data. I have plotted the coherence alongside these graphs (as shown in the first screen recording and in one of the images), and it is significantly less than 1-- starting at or below 10^(-1). As a note, I am unsure of why the raw data looks like this-- the laser goes through periods of extreme noise and I think this data was taken during one of them.
  182   Mon Jul 31 12:39:01 2023 ShaneUpdateElectronicsLED cable assemblies installed
Today I put together the two LED cable assemblies for the CyMAC and mounted them in the anti-aliasing and anti-imaging chassis.
  181   Fri Jul 28 18:03:07 2023 PamellaUpdateFLIRFinal plot - FLIR
[Pamella]
    1. I was able to plot the final result with the data to the heater. I attached below the "3Combined_HighTemp_Gaussian_Plot." in this plot we can see better behavior on the Gaussian compared to the plot in ELOG 169, I was using the same data but with a different approach. On the ELOG 169, we have the center point isolated data and this new plot is the temperature more than 70 C isolated because we have a very good heater temperature distinguish do background. For the all data I got I was using a power current of 0.20A. To get the data I waited for 30 minutes until the heater became stable and after that, I started to take snaps, I took more than one snap for each one different 6 positions on the screen, and We can see the positions on ELOG 167.
    2. Also I attached the calibration plot ("calibration_plot") between the measurements with the FLIR camera and thermocouple and we can see looks good if we compare the final plot.
    3. For better analyses I attached a plot of the calibration line on the Gaussian plot.
    4. To do: I will finish the final report.
  180   Fri Jul 28 17:45:45 2023 CelesteUpdateTCSGraphical Updates to HOM RH Modification, Friday 7/28
Updated 1/8th Heater simulation modification graphs. Slides 7, 10, 16-19 are new additions.
  179   Fri Jul 28 13:46:17 2023 AidenUpdateVACVacuum Chamber Baking Update

Took some more data to look at the HC count. Initial data was from leaving the Argon leak closed and then left it open for 15 minutes and then took data for the open scenario. Attached are the graphs for these where attachment 1 is the closed scenario and attachment 2 is the open scenario.

From these graphs it looks like the signal-noise ratio of our calibration line is poor with the ratio between these two being 1.3. This means that the calibrated leak is barely being detected over the background. This should improve with more baking and pumping. I have also now attached overlayed graphs comparing the chamber when the leak is closed versus when it is open. As well as one comparing the chamber right after the bake versus the most recent data both with the leak open.

  178   Fri Jul 28 13:39:39 2023 shaneUpdateCleanroomfull 5 zone cleanroom particle count
Here's the 5 zone cleanroom measurement from today.
  177   Fri Jul 28 13:07:39 2023 Shane, Aiden UpdateCleanroomcleanroom cleaning and particle count
[Aiden, Shane]

cleaning cleanroom and particle count

  • 11:08 am: started particle count
    • zone 3:
      • 0.3 u: 4198
      • 0.5 u: 1080
      • 1.0 u: 581
    • zone 4:
      • 0.3 u: 1247
      • 0.5 u: 623
      • 1.0 u: 415
  • 11:24 am: break for removal of vac chamber insulation (pictures attached), with counts before removal as seen above, and counts after removal/replacement for zone 3 as follows:
    • zone 3:
      • 0.3 u: 2993
      • 0.5 u: 415
      • 1.0 u: 207
  • 12:02 pm: began surface check and wipedown
  • 12:13 pm: started vacuuming the floor
  • 12:25 pm: finished vacuuming the floor
  • 12:26 pm: started mopping the floor
  • 12:32 pm: finished mopping the floor
  • 12:32 pm: started cleaning the buckets
  • 12:37 pm: started mopping with IPA wipes
  • 12:43 pm: finished mopping with IPA wipes
  • 12:45 pm: changed sticky floor mats
  • 12:47 pm: started particle count
    • zone 3:
      • 0.3 u: 2951
      • 0.5 u: 290
      • 1.0 u: 41
    • zone 4:
      • 0.3 u: 290
      • 0.5 u: 0
      • 1.0 u: 0
  176   Thu Jul 27 14:46:55 2023 Shane, JonUpdateElectronicsAA chassis DC on/off switch assembled
Made the first DC on/off switch assembly today and installed in anti-aliasing chassis. Second switch assembly to be completed later.
  175   Thu Jul 27 14:11:42 2023 SophiaUpdateScripts/ProgramsUpdate on Laser Noise Data Collection and Analysis: Dynamic CSD and PSD Plots
Here's a screen recording of the dynamic raw data and PSD/CSD plots as they are now. Will begin working on implementing a code to generate the statistical estimator for the CSD uncertainty now. (Will talk to Tyler more about whether I can get the lines to happen or not)
  174   Thu Jul 27 11:28:36 2023 Sophia UpdateScripts/ProgramsUpdate on Laser Noise Data Collection and Analysis: Dynamic CSD and PSD Plots
This week I have successfully been able to implement our dynamic CSD and PSD plotting code, but along the way I encountered a few challenges which I will outline in this elog post. Challenges: 1. Once I was able to plot the data through time, I produced a graph of the raw data (shown below in the top to images) which showed pulsed data instead of a continuous stream. On Tuesday (26th of July) Tyler and I fixed this issue, realizing that calling the starting the trigger in the red pitaya was the issue. When I commented that line of code out, it immediately started plotting continuously. 2. When that issue was solved, We then started having problems with the automatically generated lines in the python program which would double back on each new iteration. I am still dealing with this issue, because the line likes to follow the progression of the data intake instead of through the plot. Currently, I am trying to plot the data as a scatter plot and then add the line as this might make it care only about the data's distribution instead of the order of the points in the list, but I am still unsure. I might try out np.sort (or some equivalent to sort the entire data set before plotting) as well.
  173   Thu Jul 27 10:18:43 2023 CelesteUpdateTCSGraphical Updates to HOM RH Modification
Attached are updated graphs of the irradiance distribution from the 1/8th ring heater units (extruded and reduced in length).
  172   Tue Jul 25 15:35:14 2023 ShaneUpdateElectronicsMore chassis moved
Finished basic assembly of binary input and output chassis today, and moved one to top shelf of work bench. The other is in corner of work bench (image attached). They are delicate, so please do not move them or place anything on top of them.
  171   Mon Jul 24 16:19:29 2023 Shane, JonUpdateElectronicsChassis semi-assembled and moved
Began assembly on AA and AI chassis today, moved them both to top work bench shelf (image attached). They are delicate so please do not disturb them or put anything on top of them.
ELOG V3.1.3-7933898