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  Richardson Lab Experimental Log, Page 3 of 10  Not logged in ELOG logo
ID Date Author Type Categorydown Subject
  292   Fri Dec 15 14:03:02 2023 AidenHowToVACVacuum Chamber Opening
[Aiden]

1. Turn off the RGA filament and disconnect it.

2. Record the pressure and then close the angle valve and gate valve on the RGA line to isolate it from the system.

3. Turn off the backing and turbo pump and let the turbo pump spin to a stop by slowly leaking the chamber. The slower the safer.

4.Slowly open the vents on the chamber and the turbo pump. Making sure not to raise the pressure too fast.

5. Once done venting the chamber, open the lid by removing the bolts and prying the lid open with a long flat head screw driver.

6. Removed previous parts and placed them into clean bags. Place new parts inside of the chamber and group them together close to the center.

7. Place the lid back onto the chamber and tighten the bolts in a circular pattern until tightened all the way with the wrench.

8. Make sure all vents are closed and turn the backing pump back on.

9. The turbo pump can be turned back on when the pressure reaches e-1 torr.

10. Wait until the chamber reaches a pressure of e-6 torr before opening the angle and gate valve on the RGA line. After the RGA line is open and the pressure is still below e-6 torr, the RGA filament can be turned on and a leak test of the lid should be performed.

11. After the leak test shows no leaks, proceed with starting the low temp bake.

  293   Sun Dec 17 19:43:18 2023 AidenUpdateVACVac Heating Update
[Aiden]

I measured the temperature of the flanges where some of the electronics will go and I found that the RGA flange was at 55C and the two full range gauges were at 65C. I also stopped bake 9 to cool down for measurement.

  295   Mon Dec 18 15:51:49 2023 AidenUpdateVACVAC System Heating Update
After letting the chamber cool down I put the electronics back on and turned the RGA element back on. No data has been taken yet as to let the pressure continue to fall as the RGA is powered.
  296   Tue Dec 19 15:45:05 2023 AidenUpdateVACVacuum Chamber Baking Update
Took RGA data for the macor parts inside of the chamber. With the Ar open the HC levels read 30 torrl/s which is around where it was before the bake.
Attachment 1: bake9_231219_Macor_ArO.png
bake9_231219_Macor_ArO.png
Attachment 2: bake9_231219_Macor_ArC.png
bake9_231219_Macor_ArC.png
  301   Tue Jan 9 16:35:09 2024 AidenUpdateVACVAC System Leak and Heating
[Luis, Luke, Aiden]

Leak tested each flange and weld and only found two flanges to have noticeable leaks with the electron multiplier on. These were the turbo pump flange and the RGA flange that connects to the cross. The RGA one is rather new as it has not had a measurable leak before and it was around 2 e-8. We then applied the new sealant to these two flanges as directed by the instructions on the packaging.

Then after waiting a few minutes for the sealant to dry we started the bake. We got the PID controllers set to 120 after many steps and we checked the temperature of the flanges throughout this increase. The flanges never reached 70C with the electronics still left on it. The RGA was left on as well.

  306   Tue Jan 16 16:11:41 2024 AidenUpdateVAC 
[Aiden,Luis]

Below is the data for the most recent bake. I believe the chamber is cleaner than it is actually showing as the RGA data was still getting lower while the data was being taken. I will take the data again tomorrow just in case. Still, the data shows that the chamber is basically as clean as it was before bake 10 and this means further power testing can proceed.

Helium leak tested the chamber again today to check if the sealant changed anything. The two primary target flanges from last time have improved significantly with the flange from the RGA on the cross now being below 2e-14. While the turbo pump flange was leaking at a rate of 4e-13. Much better than what it has been before.

Attachment 1: bake10_240116_Elements_ArO.png
bake10_240116_Elements_ArO.png
Attachment 2: bake10_240116_Elements_ArC.png
bake10_240116_Elements_ArC.png
  308   Thu Jan 18 15:13:37 2024 AidenUpdateVACVAC Heating System Update
[Aiden]

Took more data today and the chamber and elements are showing an even lower HC level than we have gotten before. It is safe to say that the elements are not contaminated and out gassing HC into the chamber.

Attachment 1: bake10_240118_Elements_ArO.png
bake10_240118_Elements_ArO.png
Attachment 2: January_18_Ar_Open_Elements_Analyzed.png
January_18_Ar_Open_Elements_Analyzed.png
  314   Fri Feb 2 19:08:20 2024 AidenUpdateVAC1st Hot Element RGA Scan
Here are the measurements for the RGA scan of the elements while on at around 160C. The pressure of the chamber during the test was 4.12 e-8 torr.
Attachment 1: bake10_240202_Elements_ArC.png
bake10_240202_Elements_ArC.png
Attachment 2: bake10_240202_Elements_ArO.png
bake10_240202_Elements_ArO.png
  316   Mon Feb 5 14:17:52 2024 AidenUpdateVACHeater Element RGA Scan
Here are the new RGA scans for the powered Heater elements. The pressure at the time of taking data was 2.88 e-8 torr. The HC levels are at 40 e-10 torrl/s which is not bad but still higher than the lowest we have recorded.
Attachment 1: bake10_240205_Elements_ArO.png
bake10_240205_Elements_ArO.png
Attachment 2: bake10_240205_Elements_ArC.png
bake10_240205_Elements_ArC.png
  319   Thu Feb 8 17:37:48 2024 AidenUpdateVACHeater Element RGA Scan
Took more RGA data now that the heaters are powered by 18V. The pressure of the system during the data taking was 3.8 e-8 torr. The RGA scans seem to have gotten worse as well with this power increase.
Attachment 1: bake10_240208_Elements_ArO.png
bake10_240208_Elements_ArO.png
Attachment 2: bake10_240208_Elements_ArC.png
bake10_240208_Elements_ArC.png
  320   Mon Feb 12 17:35:47 2024 AidenUpdateVACHeater Element RGA Scan
Took more RGA data before and after increasing the heater elements to 300 degC and before heating them up.

Started Bake 11 as well to hopefully prevent any hydrocarbons from getting captured by the room temperature walls of the chamber. The PID controllers were set to 100C.
Attachment 1: bake10_240212_Elements_ArO.png
bake10_240212_Elements_ArO.png
Attachment 2: bake10_240212_Elements_ArC.png
bake10_240212_Elements_ArC.png
Attachment 3: bake10_240212_Elements_300C_ArC.png
bake10_240212_Elements_300C_ArC.png
  325   Tue Feb 13 12:34:04 2024 AidenUpdateVACVAC Heating System Update
Here is an overlay with for all the heating steps done with the heater elements.
Attachment 1: bake10_240118_Elements_ArO.png
bake10_240118_Elements_ArO.png
  327   Fri Feb 16 18:37:28 2024 JonUpdateVACBake ended 6:23 pm

I ended the bake of the UHV system (that began on Monday) at 6:23 pm today by switching OFF both PID controllers. The heaters elements were run at max power (24 V DC / 200 mA per element) during this bake, and I left them powered at the same level.

At the time, the instrument readings were as follows:

  • Left high-limit controller: 138 C
  • Right high-limit controller: 128 C
  • Left PID controller: 100 C
  • Right PID controller: 100 C
  • Main volume pressure: 8.17e-7 Torr
  • RGA volume pressure: 4.63e-7 Torr
  328   Mon Feb 19 14:17:50 2024 AidenUpdateVACHeater Element RGA Scan
Three days after the completion of Bake 11, the Heater elements RGA scan looks much cleaner. The HC level is back down to 33 e-10 torrl/s with the pressure at 2.13 e-8 torr. I could not take a= scan with the Argon closed as it was left open during the bake and not closed since then.
Attachment 1: bake11_240219_Elements_ArO.png
bake11_240219_Elements_ArO.png
  335   Thu Feb 22 21:48:16 2024 JonUpdateVACVacuum vent for RGA testing of reflector
[Jon, Tyler, Luke, Aiden]

Summary

Following Wednesday's cleanroom cleaning [333], we proceeded to vent the vacuum chamber, remove the heater elements and their mount structure, and install the FROSTI reflectors. The reflectors are the final components to undergo RGA testing before the FROSTI prototype can be assembled. After installing the reflectors, we pumped the chamber back down and initiated a 48-hour 125 C bake.

Vacuum Vent

At ~1:00 pm, we shut off power to all eight of the FROSTI heater elements. Prior to shutoff, all were operating in vacuum at roughly 300 C. We then waited approximately 30 minutes for the elements' temperatures to fall below 50 C.

At this point, we isolated the RGA volume from the main volume by closing both gate valves, leaving the RGA volume to continue to be pumped through the bypass line. We then backfilled the main volume via the needle valve connected to one of the 2.75" ports. Once the pressures had equalized, we removed the chamber lid via our usual procedure (requiring only a small amount of flathead-screwdriver prying) and extracted the heater element assembly.

Reflector Assembly

We then removed the FROSTI reflectors from their protective packaging (for the very first time) on the cleanroom tabletop. We tested the fit of the Macor and stainless steel hardware in the reflectors' tapped holes. The Macor standoffs and bolts appear to fit perfectly. However, the 1/4-20 tapped holes for joining the two reflector halves are too shallow by ~1/4". As a temporary fix, we used some on-hand stainless steel washers (which had already been cleaned and baked) to securely fasten the two halves together. In the final assembly we will replace these with slightly shorter 1/4-20 vented bolts.

Pumpdown and Bake

The two fastened reflector halves were placed inside the chamber, sitting on top of the two mounting legs (see attached photos). We then reinstalled the lid. In order to rough the main volume, we isolated the RGA volume from the pumpline (by closing the bypass line valve), shut down the pumps, and then backfilled the pumpline via the manual vent valve on the turbo pump.

Once the pressures had equalized, we opened the 6" gate valve separating the pumpline from the main volume and powered on the roughing pump. Once the main volume pressure fell below 0.5 Torr, we powered on the turbo pump as well. The main volume pressure reached 5e-6 Torr within ~30 minutes, consistent with previous experience, and was continuing to slowly fall.

Lastly, we initiated a 125 C bake-out of the entire system following our usual procedure. We plan to run this bake for 48 hours (i.e., through the end of the day Friday).

Attachment 1: IMG_0938.png
IMG_0938.png
Attachment 2: IMG_0939.png
IMG_0939.png
  348   Fri Mar 15 16:58:55 2024 AidenUpdateVACVacuum Chamber Frosti Testing
[Luke, Luis, Aiden] On Thursday, March 14 - Took preliminary RGA scans of the empty chamber to compare later on. Vented the chamber and placed the FROSTI into the chamber. Plugged in the DB-25 connectors into the feed through port and checked the connection to make sure there were no shorts before closing the chamber and starting the pumps again. On Friday, March 15 - The pressure in the chamber has come down to 7 e-6 torr. It seems to be coming down much slower despite the little time the chamber was left open for. This may be due to the FROSTI being out on the table for so long and a bake may be needed to bring the pressure down to near UHV.
Attachment 1: bake12_240314_Empty_ArC.png
bake12_240314_Empty_ArC.png
Attachment 2: bake12_240314_Empty_ArO.png
bake12_240314_Empty_ArO.png
  367   Mon May 13 14:48:27 2024 AidenUpdateVACNew Vacuum Chamber Design
I created a new model for the vacuum chamber based on the ideas from last week's meeting.

It should be noted that we can not have the zero length reducer and the gate valve on the same arm as they both have blind tapped holes. We need to decide if we want the gate valve or not as if we do, we will need to use the 3 inch long reducer.

Important Measurements:

From the back of the flange to the back of the RGA: 25.25 in

Height from bottom of the blank to the bottom of the chamber: 2.75 in

Attachment 1: VaccumChamberAssembly__Redesign_v5.jpg
VaccumChamberAssembly__Redesign_v5.jpg
  372   Mon Jun 3 09:24:48 2024 AidenUpdateVACVacuum Chamber Rendering
Here is a new render of the vacuum chamber that includes the 2.75 tee to place the Argon leak right next to the RGA. The conical reducer under the spherical cube was also replaced with a 4.5 blank. The height from the bottom of the blank to the bottom face of the chamber is 5.45". With the chamber now on 1" standoffs, we will need a support with a height of 6.45".
Attachment 1: VaccumChamberAssembly__Redesign_with_tee.jpg
VaccumChamberAssembly__Redesign_with_tee.jpg
Attachment 2: VaccumChamberAssembly__Redesign_with_tee_top.png
VaccumChamberAssembly__Redesign_with_tee_top.png
  384   Tue Jun 25 17:19:42 2024 LukeUpdateVACVacuum chamber leak checking
Currently our main leak is in the RGA line. We found this by closing the gate valve from the main volume to see if which side was leaking more. After identifying this we are pumping down the main volume to see how low it can go the third attachment was taken at 4:16 6/25/24. Pumping started around 3:15. We have not been able to find exactly which flange is leaking, but our guess is on the small blanks and where the cube attaches to the gate valve as seen in the second attachment. We will try a few more things and if the leak is not found/fixed we are planning on changing the configuration of the RGA line to remove the spherical cube, which we believe to be the problem. See fourth attachment for rough sketch of initial idea. We have all of the parts required and they are clean and double bagged in 1129. I have not yet made all the measurements to confirm that this design is feasible.
Attachment 1: image_2024-06-25_170036021.png
image_2024-06-25_170036021.png
Attachment 2: image_2024-06-25_170057738.png
image_2024-06-25_170057738.png
Attachment 3: image_2024-06-25_170120030.png
image_2024-06-25_170120030.png
Attachment 4: image_2024-06-25_171238788.png
image_2024-06-25_171238788.png
  386   Wed Jun 26 16:39:34 2024 LukeUpdateVACVacuum chamber leak checking
On Tuesday I had isolated the main volume and let it pump down over-night. Today, Wednesday, I checked it and it had only gone down by a small amount compared to when I left it on Tuesday. I then proceeded to tighten down the bolts attaching the tubo-pump to the zero-length reducer while it was under vacuum. This caused the pressure to drop down a few orders of magnitude.
Attachment 1: image_2024-06-26_162539705.png
image_2024-06-26_162539705.png
Attachment 2: image_2024-06-26_162601616.png
image_2024-06-26_162601616.png
  390   Fri Jun 28 18:15:16 2024 LukeUpdateVACVacuum chamber

We will be configuring the RGA line to remove the spherical cube from the system. Currently our plan for the new design is to connect a 4.5" to 2.75" Reducing Cross to the gate valve on the vacuum system. It will be orientated vertically with the turbo pump on top coming off the end will be a 90 deg elbow. On the bottom there will be a 4.5" to 2.75" Zero length reducer attached to that will be a Tee on one side the pressure sensor and the other the RGA. Connected to the elbow will be the calibrated leak. 

The only parts not readily available are the ZLR and the 2.75" gaskets

Part name Count needed Status/comment
2.75" Tee 1 In use in current RGA line
4.5" to 2.75" Reducing Cross 1 Needs to be clean and baked
4.5" to 2.75" Zero length reducer 1 To be purchased  
2.75" 90 deg elbow 1 Clean needs to be removed from another part
5/16 - 24 X 2.00" Bolts and nuts 16

8 in clean room and plenty in storage they will need to be clean and baked. Plenty of nuts in clean room.

1/4 - 28 X 1.25" Bolts and nutplates 24 12 in use in RGA line and 12 in storage that will need to be clean and baked. Sufficient nutplates in clean room
1/4 - 28 X 7/8" Bolts  12 Plenty of bolts in clean room
2.75" Copper Gasket   6 5 gaskets in clean room and none in storage. So some will need to be purchased
4.5" Copper Gasket 2 About 10 in clean room 
  400   Wed Jul 10 17:31:07 2024 LukeUpdateVACRGA line disassembly and upgrade

[ Luke, Cynthia, Michael, Xuesi, Anthony ]

Started work around 12:45

We vented the chamber first and once it reached atmospheric pressure we started taking apart the RGA line.

We removed the parts in this order: Calibrated leak, RGA, Pressure gauge, 2.75" Blank on Tee, 2.75" Tee, all 1.33" Blanks on the cube, 4.5" feed through port, and finally the cube. Everything went smoothly after every part was taken off we covered the ends in Aluminum foil to maintain cleanliness. 

We then started the assembly of the new line. The parts were added in this order: Reducing cross, ZLR, Tee, Cal leak, RGA, 90 deg Elbow, and Pressure sensor.

We left off the Turbo pump as of now because we weren't able to find a 1" post not in use and we didn't want to put too much weight on the cross. We also noticed that the RGA might not fit on its probes because of a slight tilt to the cross and by extension the Tee. If this ends up being a problem we might need to remove all the parts connected to the cross so that we can reposition it so that the 2.75" rotating flange is connected to the gate valve.

Ended work around 4:00

Attachment 1: image_2024-07-10_172112210.png
image_2024-07-10_172112210.png
Attachment 2: image_2024-07-10_172431863.png
image_2024-07-10_172431863.png
Attachment 3: image_2024-07-10_172603090.png
image_2024-07-10_172603090.png
Attachment 4: image_2024-07-10_172823966.png
image_2024-07-10_172823966.png
  401   Thu Jul 11 15:53:39 2024 LukeUpdateVACRGA line upgrade

[ Luke, Jon ]

Started work at 11:00

As mentioned in my previous post the RGA was not clearing the table because of a tilt in the cross. So I removed the 90 deg elbow, loosened the bolt securing the Tee to the ZLR, and removed the cross from the gate valve. I then spun around the Tee on the bottom so that the cal leak would be pointing in the right direction and connected the rotating 2.75" flange of the cross to the gate valve. I then added the small turbo pump to the top of the cross. 

Then with the help of Dr. Richardson, we made some adjustments to how the Tee was oriented with respect to the cross and how the cross was with respect to the table. So that the cal leak and RGA would fit on the table. After that we made some changes to the bolting of the ZLR to reducing cross replacing the 2.00" bolts and nuts with 1.75" bolts and nut plates. We did face some difficulty with half of the 2.00" bolts which required a bit of torque to get them out. 

Finished work at 2:20 

 

Things to do:

Before we start pumping down the system again Dr. Richardson wanted two other changes to be made. To replace the 2.75" to 1.33" conical reducer with a zero length reducer. He also wants the bolts that hold the main turbo pump to be replaced with nut plates. 

I plan on starting this work on Friday (7/12) before pumping down over the weekend

Attachment 1: image_2024-07-11_154630323.png
image_2024-07-11_154630323.png
Attachment 2: image_2024-07-11_154818191.png
image_2024-07-11_154818191.png
Attachment 3: image_2024-07-11_154902840.png
image_2024-07-11_154902840.png
  405   Mon Jul 15 13:30:49 2024 Luke UpdateVACProblem with 2.75" to 1.33" zero length reducer
Last Friday while checking the depth of the ZLR I got one of the screws stuck. Today I tried a couple things to get it out. First I tried a few different pliers to be able to grip lower on the screw this didn't work. So I switched to the other method of drilling a small hole to see if maybe the threads would pull away from the walls of the hole a bit. This kind of worked as seen in the picture below I was able to remove most of the screw but there is a bit still stuck which I was not able to remove and I didn't want to use a larger bit for fear of damaging the tapped hole.
Attachment 1: IMG_1882.jpg
IMG_1882.jpg
  411   Mon Jul 22 18:19:34 2024 LukeUpdateVACZero length reducer stuck bolts

Today, I borrowed a bolt extractor drill bit from the machine shop to remove some stuck bolts from the zlr. Before starting, I laid down a sheet of aluminum foil on the work table and wiped down all the tools I was going to use. I began by drilling a small pilot hole and then enlarged it with a 5/32 drill bit. However, when I attempted to use the bolt extractor, it didn't grip the bolt effectively. Our bolts were too seized, causing the extractor bit to repeatedly slip instead of gaining traction.

Attachment 1: image_2024-07-22_181607501.png
image_2024-07-22_181607501.png
Attachment 2: image_2024-07-22_181632965.png
image_2024-07-22_181632965.png
  425   Fri Aug 16 12:51:46 2024 Luis MartinUpdateVACUpdate on vacuum chamber status

[Luis, Luke, Tyler]

Vacuum chamber parts were finally received and assembled. After whipping down the parts, the blank was removed from the reducing cross. Then, the zero-length reducer was attached. Lastly, we installed the T that had the argon leak and RGA. The final pump down showed signs of an improved seal since the pressure dropped quite fast. This pressure is well bellow the limit required to use the RGA, argon test leak could be performed some time next week.

Attachment 1: IMG_1910.HEIC
Attachment 2: IMG_1911.HEIC
Attachment 3: IMG_1909.HEIC
Attachment 4: IMG_1912.HEIC
  427   Fri Aug 23 16:08:32 2024 LukeUpdateVACRGA line leak testing

[Luke, Luis, Jon, Tyler]

On the 22nd Dr. Richardson showed Luis, Tyler and I how to preform a leak test with the RGA. We did the initiall test and found a few leaks two were particuarly bad highlighted in orenge below. To try and remidy this we planned on replacing the copper gaskests on the leaking flanges. We then began taking the two problem flanges off, but seven of the eight bolts holding on the turbo pump were over tightened and had seized. So after we got them off we postponed the rest of the work to the next day.

On the 23nd Luis and I reattached the badly leaking flanges with new copper gaskets. We then preformed the Helium leak test with the RGA. As seen in the table below we weren't able to majorly changed the leaks in the two flanges.

 

Connection Initial  After disassembly
Tee - RGA 3.1e-9 -> 2.4e-9 9.2e-9
Tee - Cal leak Low Low
Tee - ZLR (2.75"-4.5") Low 9.2e-9
ZLR (2.75"-4.5") - Reducing Cross 2.1e-8 -> 1.9e-8 3.6e-8 -> 9.3e-9
Cross - Elbow Low 1.2e-9
Elbow - Pressure sensor Low 2.9e-9
Cross - Turbo pump (small) 2.1e-8 -> 3.1e-8 6.9e-8 -> 2.2e-8
Cross - Gate valve Low Low
Gate valve - Port 2.4e-9 -> 2.2e-9 1.2e-9
Port - ZLR (6.0"-8") 1.1e-9 N/A
ZLR (6.0"-8") - Turbo pump (large) Low N/A
Port - Pressure sensor Low N/A
Port - Up to air valve Low N/A
Port - Blank Low N/A
Port - Feed though  port Low N/A
Lid Low N/A

 

  429   Tue Aug 27 15:01:26 2024 LukeUpdateVACRGA line leak testing

[Luke, Tyler]

On the 27th Tyler and I ran the RGA leak test again with the electron multiplier on. These were the leaks we measured. The chamber's overall pressure was at ~6e-8 torr. 

Connection Leak rate (torr)
Tee - RGA 3.92e-11 (very low)
Tee - Cal leak 4.77e-11 (very low)
Tee - ZLR (2.75"-4.5") 4.97e-11 (very low)
ZLR (2.75"-4.5") - Reducing Cross 2.45e-9   (low)
Cross - Elbow 7.36e-11 (very low)
Elbow - Pressure sensor 2.36e-11 (very low)
Cross - Turbo pump (small) 8.07e-9   (lowish)
Cross - Gate valve 4.02e-11 (very low)
Gate valve - Port 2.27e-9   (low)
Port - ZLR (6.0"-8") 1.11e-9   (low)
ZLR (6.0"-8") - Turbo pump (large) 1.00e-10 (very low)
Port - Pressure sensor 1.05e-10 (very low)
Port - Up to air valve 1.08e-11 (very low)
Port - Blank 5.58e-10 (very low)
Port - Feed though port 1.21e-11 (very low)
Lid 1.11e-11 (very low)

 

 

  431   Thu Aug 29 16:39:34 2024 LukeUpdateVACPhotos of heater tape
Attachment 1: IMG_2052.jpeg
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Attachment 2: IMG_2051.jpeg
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Attachment 3: IMG_2048.jpeg
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Attachment 4: IMG_2047.jpeg
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Attachment 5: IMG_2046.jpeg
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Attachment 6: IMG_2044.jpeg
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  432   Sun Sep 1 16:17:40 2024 LukeUpdateVACVacuum chamber leak checking and re-applying heating tape

[Luke, Luis, Cinthia, Michal, Tyler]

On the 26th Cinthia, Michal, and I took off the insolation on the vacuum chamber and re-routed it to include the new RGA volume. 

The next day Luis and I finished up the last of the flanges to be attached. We attached the Pirani gauge with a conical reducing nipple to the 2.75" port on the vacuum chamber. We then preformed the Helium leak testing, both flanges were quite low the 2.75" flange had a leak of 1.68e-10 torr and the 1.33" flange of 5.5e-12 torr. The leak on the 1.33" flange was so low it was difficult to know how much of it was real and how much was just noise.

  433   Tue Sep 3 15:52:56 2024 LukeUpdateVACHeater tape initilization

[Luke, Tyler, Jon]

On the 3rd we set up the pid controllers for the heater tapes and after putting on the insulation we started heating them up. We first brought it to ~50C and let it stabilize, there was about a 6-7 degree difference between the RGA and the barrel temperature, with the barrel being higher. We then brought it to 60 then 70C it still maintained the slight difference between the RGA and barrel temperatures.

Here is a table of the temperatures of the flanges connected to electronics as I left it.

Electronics Temperature (C)
Pressure gauge (Main volume) 58
Main turbo pump 45
RGA 37
Pressure gauge (RGA volume) 39
Cal leak 40
Mini tubo pump 36
Pirani gauge 37

Notes: I removed the electronics from the pressure gauge (main volume) because while it was below the required threshold it was still quite high compared to the other flanges.

  435   Fri Sep 6 14:34:52 2024 Luke UpdateVACHeating tape work

On the 5th I had tried to start baking the vacuum chamber however certain parts of the chamber were getting too hot and causing the controllers to shut off. So I turned them off so that the next day I could rearrange the temperature probes. I then on the 6th set them up so that instead of overshooting the temperature they would be a little low in places.

After being left over night the cooler parts of the vacuum chamber got much closer to the desired temperature of 120C.

Here is a table of the temperatures of the sections of the chamber. Note: After these measurements were taken the PID controllers were set to 125C.

Location   Temperature (C)
Lid (PID controller 1 emergency shutoff) 108
Barrel lower (PID controller 1) 120 
Barrel upper (PID controller 2 emergency shutoff) 118
RGA volume (PID controller 2) 120

Here is a table of temperature of the flanges that have electronics.

Electronics Temperature (C)
Pressure gauge (Main volume) 79
Main turbo pump 64
RGA 51
Pressure gauge (RGA volume) 55
Cal leak 47
Mini turbo pump 50
Pirani gauge 45 

Other temperatures of note:

The optical table was about 38C

The cleanroom was around 33C (~91F)

  438   Mon Sep 9 21:02:37 2024 LukeUpdateVACSteadystate temperature of flanges

I measured the temperature of the flanges and reconnected the RGA turning on its filament. I then turned off the PID controllers.

Here is a table that has the temperature of the different parts of the vacuum chamber.

Electronics Temperature (C)
Pressure gauge (Main volume) 81
Main turbo pump 67
RGA 53
Pressure gauge (RGA volume) 60
Cal leak 48
Mini tubo pump 46
Pirani gauge (1.33") 46
conical nipple (2.75") 82
Lid 112
Barrel lower 125
Barrel upper 122
RGA volume 125
Bottom of chamber 117
  440   Mon Sep 16 13:51:23 2024 Luis MartinUpdateVACRGA Scans

[Luis, Luke}

Three RGA scans were taken. The improvement in the amount of HC in the vacuum is visible across the different measurements. Images are attached.

Attachment 1: 2024-09-11_PostBake1_ArO.png
2024-09-11_PostBake1_ArO.png
Attachment 2: 2024-09-13_PostBake1_ArO.png
2024-09-13_PostBake1_ArO.png
Attachment 3: 2024-09-16_PostBake1_ArO.png
2024-09-16_PostBake1_ArO.png
  448   Wed Sep 25 09:06:09 2024 Luis MartinUpdateVACRGA Scans
RGA Scan Comparison

The following images compare the RGA scans from 9/23/24, after the first bake with the new vacuum system, with those from 3/14/24, after bake 12 with the old system.

The first image shows a graph of the raw data and includes the calibrated leak for both curves. As we can see, our new system meets LIGO standards of cleanliness.

The second graph contains the plot of the normalized data.

Attachment 1: 24overlay.png
24overlay.png
Attachment 2: 24overlayNormalized.png
24overlayNormalized.png
  459   Wed Oct 16 13:58:59 2024 Luis MartinUpdateVACRGA Scan

The following figure displays data acquired on 10/09, and it shows that we are no longer below the cleanliness standard. Also, the system's pressure went up to 1.9x10-8 Torr (approximately 7x10-9 Torr previously). This might be due to a leak somewhere in the system. More tests will be performed later.

Attachment 1: 2024-10-09_PostBake1_ArO.png
2024-10-09_PostBake1_ArO.png
  462   Wed Oct 23 11:48:06 2024 Luis MartinUpdateVACLeak Test Results

[Luke, Luis, Mary, Ma]

On 10/22/24 Luke, Ma, Mary and myself ran a leak test, the results are displayed below. The overall pressure of the vacuum was 2.0e-8 and the temperature readings were 26C for the RGA and 25C for the main volume.

Connection Leak rate (torr)
Tee - RGA 9.4e-12 (very low)
Tee - Cal leak 1.58e-11 (very low)
Tee - ZLR (2.75"-4.5") 7.32e-12 (very low)
ZLR (2.75"-4.5") - Reducing Cross 6.9e-11   (low)
Cross - Elbow 2.34e-11 (very low)
Elbow - Pressure sensor 1.96e-11 (very low)
Cross - Turbo pump (small) 1.91e-9   (lowish)
Cross - Gate valve 1.66e-10 (very low)
Gate valve - Port 7.41e-10   (low)
Port - ZLR (6.0"-8") 2.93e-10   (low)
ZLR (6.0"-8") - Turbo pump (large) 6.15e-11 (very low)
Port - Pressure sensor 2.0e-11 (very low)
Port - Up to air valve 1.42e-11 (very low)
Port - Blank 1.27e-11 (very low)
Port - Feed through port 4.59e-12 (very low)
Lid - Curtain side 3.09e-11 (very low)
Lid - Wall side 4.26e-11 (very low)

 

 

  463   Wed Oct 23 12:08:36 2024 Luis MartinUpdateVACRGA Scan

[Luke, Luis, Mary, Ma]

On 10/22/24 Luke, Ma, Mary and myself ran a RGA scan, the results are displayed below. The overall pressure of the vacuum was 2.0e-8 and the temperature readings were 26C for the RGA and 25C for the main volume.

As we can see, the vacuum is passing cleanliness standards again.

Attachment 1: 2024-10-22_PostBake1_ArO.png
2024-10-22_PostBake1_ArO.png
  468   Tue Nov 5 11:08:40 2024 Luis MartinUpdateVACISO Test

[Luis, Luke, Ma Michael]

The isolation test was conducted on the vacuum system. Every pump was turned off under vacuum, and pressure measurements were taken every minute for 15 minutes. The results are displayed in the sheet linked at the end of this report. The pressure of the main volume dropped very slowly.

The pressure of the RGA Volume dropped in an exponential manner. The test had to be paused at 11 minutes due to concerns about the pressure exceeding the lowest permitted level for the RGA filament.

After the ISO test was performed, we attempted to tighten the bolts of the small turbo pump on the RGA Volume. However, we noticed that the pressure had increased by nearly an order of magnitude, going from 3.27 × 10-9 Torr to 1.45 × 10-8 Torr when both volumes were separated. We conducted a leak test for that particular flange and found a concerning leak of 2.15 × 10-8 Torr, which had previously been 1.9 × 10-9 Torr. We believe the copper seal was damaged during the ISO test.

View the results sheet

  474   Tue Nov 19 17:10:34 2024 Luke UpdateVACLeak check

Chamber temperature: 23C

Chamber Initial Pressure: ~1.8e-8 main, ~3.5e-8 rga

Did another leak test after monday's work to check how the seal was holding up initial leak was 5.5e-9. I then tried to tighten the bolts a bit more the leak rose to 1.9e-8 about a factor of 4 change.

I checked another flange to confirm that I was preforming the test properly. I measured the elbow to pressure sensor to be 2.2e-11 aproximatly what it was earlier in the month (1.9e-11). 

I ran another isolation test. It is still exponetial. Graph attached.

Thoughts:

I belive at this point that it is a knife edge issue when replacing the gasket I checked both flanges and the new gasket. The tp knife edge seemed perfectly fine, the gasket had very minor scratches, and the reducing cross had very small imperfections on its edge. 

We may want to try and use the liquid sealant or get annealed gaskets for 4.5"

Attachment 1: image.png
image.png
Attachment 2: IMG_5116.jpeg
IMG_5116.jpeg
Attachment 3: IMG_5117.jpeg
IMG_5117.jpeg
  476   Wed Nov 20 12:31:24 2024 LuisUpdateVACLeak test RGA Scan after vacuum repairs

[Luke, Luis]

After the gasket replacement performed on Monday (11/18/24) we let the vacuum pump down to UHV pressure for a couple days. Today (11/20/24) we measured the pressure to be 5.30*e^-9 with a temperature of 22C, and we performed a leak test and RGA Scan.

Here are the results:

Connection Leak rate (torr)
Reducing Cross - TP Left 4.5e-9 (lowish)
Reducing Cross - TP Right 6.0e-9 (lowish)

 

 

Attachment 1: 2024-11-20_PostBake1_ArO.png
2024-11-20_PostBake1_ArO.png
  11   Mon Oct 3 17:21:39 2022 CaoUpdateTCSInspection of macor parts
The macor parts arrived and inspected today. These include:
  1. Macor spacer (drawing: LIGO_Redesign_Macor_Spacer_Drawing_v4.pdf attached below), quantities: 40
    • No defects, damages observed
    • Parts are free from grease/ machining fluid
    • Wall thickness of 1 mm appear to provide sufficient stiffness to part
    • Images of parts: Macor_spacer_0.jpg, Macor_spacer_1.jpg
  2. Macor 5-40 UNC screw (drawing: LIGO_Redesign_Macor_Screw_Drawing_v6.pdf attached below), quantities: 20
    • One screw broke, location of break: should edge between head and shaft (see image Macor_screw_5.jpg )
    • All other screws look ok, no damage observed, clean surface overall
    • Images: Macor_screw_0.jpg , Macor_screw_4.jpg
Attachment 1: LIGO_Redesign_Macor_Spacer_Drawing_v4.pdf
LIGO_Redesign_Macor_Spacer_Drawing_v4.pdf
Attachment 2: Macor_spacer_0.jpg
Macor_spacer_0.jpg
Attachment 3: Macor_spacer_1.jpg
Macor_spacer_1.jpg
Attachment 4: LIGO_Redesign_Macor_Screw_Drawing_v6.pdf
LIGO_Redesign_Macor_Screw_Drawing_v6.pdf
Attachment 5: Macor_screw_5.jpg
Macor_screw_5.jpg
Attachment 6: Macor_screw_0.jpg
Macor_screw_0.jpg
Attachment 7: Macor_screw_4.jpg
Macor_screw_4.jpg
  173   Thu Jul 27 10:18:43 2023 CelesteUpdateTCSGraphical Updates to HOM RH Modification
Attached are updated graphs of the irradiance distribution from the 1/8th ring heater units (extruded and reduced in length).
Attachment 1: HOM_RH_1_8_Unit_Modification_Graphs.pdf
HOM_RH_1_8_Unit_Modification_Graphs.pdf
  180   Fri Jul 28 17:45:45 2023 CelesteUpdateTCSGraphical Updates to HOM RH Modification, Friday 7/28
Updated 1/8th Heater simulation modification graphs. Slides 7, 10, 16-19 are new additions.
Attachment 1: HOM_RH_Simulation_Progress.pdf
HOM_RH_Simulation_Progress.pdf
  187   Tue Aug 1 16:22:35 2023 CelesteUpdateTCSGraphical Updates to HOM RH Modification, Tuesday 8/1
Slides 20-33 are newly added (data/graphs from parameter sweep feature-1/8th heater unit length varied from 10% of original to 100% of original).
Attachment 1: HOM_RH_Simulation_Progress_80123.pdf
HOM_RH_Simulation_Progress_80123.pdf
  200   Thu Aug 10 14:13:38 2023 CelesteUpdateTCS8/10/23, Simulation Graphical Progress
Attachment 1: Simulation_Progress__8_10_23.pdf
Simulation_Progress__8_10_23.pdf
  204   Fri Aug 11 10:57:20 2023 CelesteUpdateTCS8/11/23 Simulation Progress
Attachment 1: Simulation_Progress__1_32nd_Model_(1).pdf
Simulation_Progress__1_32nd_Model_(1).pdf
  209   Tue Aug 15 16:10:06 2023 CelesteUpdateTCS8/15/2023 Simulation Progress
Attachment 1: Simulation_Progress__1_32nd_Model_(2).pdf
Simulation_Progress__1_32nd_Model_(2).pdf
  291   Mon Dec 11 16:20:17 2023 JonSummaryTCSFROSTI Assembly Procedure

Below is the procedure we will follow to assemble the FROSTI prototype.

  1. Install SS guide rods and bottom Macor spacers in bottom reflector
  2. Install AlN elements on top of bottom Macor spacers
  3. Install upper Macor spacers on top of AlN elements
  4. Feed unterminated power and RTD leads through slots in upper reflector
  5. Install upper reflector, using guide rods to slowly lower into position
  6. Install vented SS bolts for reflectors; Macor bolts for heater elements
  7. Remove SS guide rods
  8. Bundle power and sensing cable with PEEK cable ties and SS cable mounts
  9. Terminate power and sensing cable bundles with PEEK DB25M connectors
  341   Mon Feb 26 21:23:27 2024 JonUpdateTCSFROSTI Assembly - Day 1
[Jon, Tyler, Luis, Luke, Mohak, Cynthia, Michael, Aiden]

FROSTI assembly began today. After a final set of RGA scans were taken, the vacuum chamber was vented and the reflectors were removed. The chamber was then resealed and pumped down again. 

Today we completed the installation of the Macor hardware and heater elements between the two reflector halves. Tomorrow we will route, bundle, and terminate the power and sensor cables. 

Attachment 1: IMG-20240226-WA0008.jpg
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Attachment 2: IMG-20240226-WA0006.jpg
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Attachment 3: IMG-20240226-WA0011.jpg
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Attachment 4: IMG-20240226-WA0010.jpg
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Attachment 5: IMG-20240226-WA0012.jpg
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Attachment 6: IMG_0944.png
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Attachment 7: IMG_0946.png
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