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  Richardson Lab Experimental Log, Page 6 of 11  Not logged in ELOG logo
ID Date Authordown Type Category Subject
  436   Mon Sep 9 12:36:45 2024 MichaelUpdateInterferometer SimulationsUpdate on Analysis of Mode Mismatch Minimization in A#
I have taken a closer look at the solution curve in the mirror parameter space which I have searched, focusing on the "resilience" of specific points, with the plan to analyze how certain conditions of the interferometer change as we move along this solution curve.
  482   Mon Dec 2 00:11:23 2024 MichaelUpdateInterferometer SimulationsStatus Update on Toroidal Mirrors Project Work
As it has been significant time from my last update on this project, I compiled a few notes about what I have been working on, current issues, and my future plans. The past few weeks have been focused on me attempting to obtain a reliable symbolic expression for mismatch. This is important going forward as it allows us to determine optimal points in the parameter space and the surrounding behavior efficiently without significant computational cost. However this been quite difficult since I've encountered some fundamental discrepancies in the way values like the ABCD matrix and q-parameters are calculated/returned in Finesse. Since I have yet to resolve this, I'm focusing on next steps in developing tools for statistical simulations.

Update Slides

  523   Tue Feb 25 01:37:00 2025 MichaelUpdateInterferometer SimulationsUpdates and Current Next Steps for Toroidal Mirrors Project
Since the previous discussion of this project, I've worked on building finesse models to verify mathematical results which model the astigmatism in a two mirror system which we attempt to minimize. This left us with a single condition for an output non-astigmatic beam. However, as can be seen in finesse simulations, there does exist other configurations which have a negligibly small astigmatism, which we may want to consider. Below I've attached the link to my overleaf project which has some updated information which I plan on discussing.

https://www.overleaf.com/project/67968921426e61d5b2fd8c96
  541   Sun Mar 23 15:39:06 2025 Luke JohnsonUpdateScripts/ProgramsRingheater Location optimization
Attached are some plots that show a new parameter sweep with a finer mesh then before. I have also been able to get a heatmap of power of HOMs in a very simple finesse model.
  543   Mon Mar 31 11:26:45 2025 Luke JohnsonUpdateScripts/ProgramsHeatmaps of power delivery performance
These plots show the required temperature to release 100W of power and the efficiency of a particular configuration with half-width w and distance away from the barrel z. I want to add to these heat maps a limit line that has restricts the proximity of the reflectors from the barrel.
  405   Mon Jul 15 13:30:49 2024 Luke UpdateVACProblem with 2.75" to 1.33" zero length reducer
Last Friday while checking the depth of the ZLR I got one of the screws stuck. Today I tried a couple things to get it out. First I tried a few different pliers to be able to grip lower on the screw this didn't work. So I switched to the other method of drilling a small hole to see if maybe the threads would pull away from the walls of the hole a bit. This kind of worked as seen in the picture below I was able to remove most of the screw but there is a bit still stuck which I was not able to remove and I didn't want to use a larger bit for fear of damaging the tapped hole.
  423   Mon Aug 12 16:35:30 2024 Luke Update Ringheater modeling Update
  435   Fri Sep 6 14:34:52 2024 Luke UpdateVACHeating tape work

On the 5th I had tried to start baking the vacuum chamber however certain parts of the chamber were getting too hot and causing the controllers to shut off. So I turned them off so that the next day I could rearrange the temperature probes. I then on the 6th set them up so that instead of overshooting the temperature they would be a little low in places.

After being left over night the cooler parts of the vacuum chamber got much closer to the desired temperature of 120C.

Here is a table of the temperatures of the sections of the chamber. Note: After these measurements were taken the PID controllers were set to 125C.

Location   Temperature (C)
Lid (PID controller 1 emergency shutoff) 108
Barrel lower (PID controller 1) 120 
Barrel upper (PID controller 2 emergency shutoff) 118
RGA volume (PID controller 2) 120

Here is a table of temperature of the flanges that have electronics.

Electronics Temperature (C)
Pressure gauge (Main volume) 79
Main turbo pump 64
RGA 51
Pressure gauge (RGA volume) 55
Cal leak 47
Mini turbo pump 50
Pirani gauge 45 

Other temperatures of note:

The optical table was about 38C

The cleanroom was around 33C (~91F)

  452   Wed Oct 2 12:05:42 2024 Luke Update Ringheater modeling Update

Power point slides

  Draft   Wed Oct 23 12:33:54 2024 Luke Update Zernike calculation update

PowerPoint slides new

PowerPoint slides older

  471   Wed Nov 13 14:06:00 2024 Luke UpdateGeneral 

slides

  472   Thu Nov 14 10:46:20 2024 Luke SummaryCleanroomCleanroom cleaning

 

[Luke, Luis, Michael]

cleaning cleanroom and particle count

  • 8:30 am: started particle count
    • zone 3:
      • 0.3 u: 1195
      • 0.5 u: 177
      • 1.0 u: 132
    • zone 4:
      • 0.3 u: 619
      • 0.5 u: 0
      • 1.0 u: 0
  • 9:00 am: began surface check and wipedown, including softwalls
  • 9:35 am: started vacuuming the floor
  • 9:43 am: finished vacuuming the floor
  • 9:45 am: started mopping the floor
  • 9:55 am: finished mopping the floor
  • 9:56 am: started cleaning the buckets
  • 10:00 am: started mopping with IPA wipes
  • 10:05 am: finished mopping with IPA wipes
  • 10:20m: started particle count
    • zone 3:
      • 0.3 u: 2213
      • 0.5 u: 398
      • 1.0 u: 0
    • zone 4:
      • 0.3 u: 1150
      • 0.5 u: 177
      • 1.0 u: 44
  474   Tue Nov 19 17:10:34 2024 Luke UpdateVACLeak check

Chamber temperature: 23C

Chamber Initial Pressure: ~1.8e-8 main, ~3.5e-8 rga

Did another leak test after monday's work to check how the seal was holding up initial leak was 5.5e-9. I then tried to tighten the bolts a bit more the leak rose to 1.9e-8 about a factor of 4 change.

I checked another flange to confirm that I was preforming the test properly. I measured the elbow to pressure sensor to be 2.2e-11 aproximatly what it was earlier in the month (1.9e-11). 

I ran another isolation test. It is still exponetial. Graph attached.

Thoughts:

I belive at this point that it is a knife edge issue when replacing the gasket I checked both flanges and the new gasket. The tp knife edge seemed perfectly fine, the gasket had very minor scratches, and the reducing cross had very small imperfections on its edge. 

We may want to try and use the liquid sealant or get annealed gaskets for 4.5"

  478   Wed Nov 27 12:27:45 2024 Luke SummaryVACSummary of vacuum work

[Luke, Luis]

Update of current state of vacuum chamber

Current temp: 24°C

Current pressure: Main 1.77e-8, RGA 5.3e-9 [torr] (Gate valve open)

Summary of recent work-->

To try and reduce the leak in the turbo pump by reducing cross-connection, we replaced the copper gasket. This made no improvement to the leaks.

Initially: 1.9e-9 --->

Left side: 1.33e-9, Right side: 3.37e-9 (Gate valve open)

This is still a significant leak. We have tried to tighten the bolts further, but they are as tight as reasonably possible. 

Things of note: While examining the knife edges, we found some very slight imperfections on the reducing cross's flange as seen in 474. This could be the source of our leak. We have replaced this gasket 1-2 times already and consistently have a slight leak. This imperfection is on the right side of the flange, which would be consistent with the measurements above. 

Unless we want to use the liquid sealant or replace the gasket with an annealed gasket, we could try baking the system again, as this allowed us to reach UHV in the main volume before. It also allowed us to pass the RGA scan, which we are currently failing. (see attached)

  480   Wed Nov 27 16:23:58 2024 Luke UpdateVACStarted bake

[Luke, Luis]

The vacuum chamber is currently baking. 

We stepped up to 125°C by increments of 30°C starting at 60°C. Everything went fine. After about 20 minutes of the PID controllers being set to 125°C, the flange closest to the RGA was 38°C, so we left it connected. 

Current state as of 4:15:

The gate valve is open, and the filament of the RGA is on.

The temperatures are as follows:

PID right barrel upper: 105°C,  RGA volume: 125°C

PID left barrel lower: 125°C, Lid: 82°C

The lower temperatures should climb as the whole system heats up. 

I will come in Saturday afternoon to turn them off so that we can look at the pressures on Monday. 

  483   Mon Dec 2 13:35:45 2024 Luke UpdateGeneralClean and bake of Viton O-rings

[Luke, Luis]

We couldn't access the bake log on the wiki. (see attached) So we looked in the documentation provided on the DCC to find at what temperature to bake the Viton O-rings. We found that we should bake Viton at 180°C for 24 hours. 

So we sonic-washed the O-rings, dried them, and then put them in the oven set to the following:

100°C in 15 minutes

100°C for 30 minutes

180°C in 30 minutes

180°C for 24 hours

30°C in 2 hours

 

Other things of note:

We refilled the water container as it was running out.

The nitrogen used to dry the clean and baked objects is now critically low.

The helium used in leak testing is also quite low (~400 psi).

 

Regarding the vacuum chamber:

I reattached the pressure gauges to the chamber and gave them about an hour to stabilize. They read out main 8.7e-9, RGA 2.6e-9. Please note these pressures should lower more as we only stopped baking on Saturday afternoon. 

  497   Wed Jan 8 17:35:57 2025 Luke SummaryCleanroomCleanroom cleaning

[Luke, Tyler, Cynthia, Shane, Michael]

Summary of Cleaning Activities:

We began cleaning Room 1119 at 2:00 PM.

At 2:30 PM, we moved to Room 1129 and continued cleaning.

Cleaning tasks included wiping down dust-collecting surfaces and vacuuming the floors.

Once the labs were clean, we proceeded to the cleanroom. 

  • Wiping down surfaces and soft walls
  • Vacuuming, mopping the floor, and finishing with IPA wipes

Particle Count Measurements:

  • Pre-cleaning (2:30 PM):
    • Zone 3:
      • 0.3 µm: 973
      • 0.5 µm: 354
      • 1.0 µm: 132
    • Zone 4:
      • 0.3 µm: 486
      • 0.5 µm: 177
      • 1.0 µm: 0
  • Post-cleaning (4:10 PM):
    • Zone 3:
      • 0.3 µm: 619
      • 0.5 µm: 132
      • 1.0 µm: 0
    • Zone 4:
      • 0.3 µm: 397
      • 0.5 µm: 0
      • 1.0 µm: 0

 

  500   Tue Jan 21 10:12:02 2025 Luke SummaryGeneralFrosti toy model

[Luke, Liu]

Over the winter break I have been working on this desmos toy model of the Frosti. There are still a few rough spots but I belive that it is a good visual representation of a 2D slice of the frosti. 

  502   Sat Jan 25 18:19:39 2025 Luke UpdateGeneralRingheater modeling Update

Here is a quick update on some of the things I have been working on regarding my project. 

  507   Sat Feb 1 17:25:52 2025 Luke SummaryGeneralCleanroom cleaning

[Luke, Cece, Luis]

Particle Count Measurements:

  • Pre-cleaning (12:15 PM):
    • Zone 3:
      • 0.3 µm: 1325
      • 0.5 µm: 265
      • 1.0 µm: 0
    • Zone 4:
      • 0.3 µm: 618
      • 0.5 µm: 132
      • 1.0 µm: 44
  • Started Cleaning (3:20 pm)
  • Finished Cleaning (4:20 pm)
  • Post-cleaning (4:35 PM):
    • Zone 3:
      • 0.3 µm: 1106
      • 0.5 µm: 221
      • 1.0 µm: 0
    • Zone 4:
      • 0.3 µm: 530
      • 0.5 µm: 44
      • 1.0 µm: 0

 

  509   Fri Feb 7 12:25:56 2025 Luke SummaryVACStarted bake

[Luke, Luis]

The vacuum chamber is currently baking. 

We stepped up to 120°C by increments of 30°C starting at 60°C. We took about an hour break at 90°C to let the temperatures equilibrate.  

Current state as of 12:20:

The gate valve is open, the calibrated Argon leak is open, and the filament of the RGA is on.

The temperatures are as follows:

PID right barrel upper: 113°C,  RGA volume: 120°C

PID left barrel lower: 121°C, Lid: 114°C

The lower temperatures should climb as the whole system heats up. 

 

  513   Sun Feb 16 16:45:18 2025 Luke UpdateGeneralRingheater position optimization

Over the last couple weeks I have been working on finding the optimal position of the ringheater's thermal profile. 

Today I would like to give an update of where I am at and my next steps.

Using the python COMSOL interface I have been able to run and save deformation data sweeping through a great deal of potential combinations of widths and positions.

I then calculated their zernike coefficients and using a very simple "quality" function (02 - (40)*10 - (4-4)*10), where 02 stands for the zernike mode of quadratic deformation, I was able to generate a heat map of comparing the "quality" verses the width and position used. 

Seen below are four plots. The first is simply the 02 coefficient of the decomposition followed by the negative of 40 and 4-4 then the "quality."

This 'quality' function was an arbitrary choice on my part. I believe that my next step would either be defining a more useful function or using finesse to model the actual effects of this surface deformation.

  517   Tue Feb 18 11:19:13 2025 Luke ConfigurationVACRepositioning of the lid's temperature probe
Before the recent bake I slightly repositioned the temperature probe on the lid from beside the heater tape to under the heater tape. This was done to better know and control the temperatures of the chamber while baking. It has appeared to work with the temperatures being held very close to the 120C target.
  520   Sun Feb 23 12:11:43 2025 Luke SummaryCleanroomCleanroom cleaning

[Luke, Mary, Luis]

Particle Count Measurements:

  • Pre-cleaning (8:40 am):
    • Zone 3:
      • 0.3 µm: 441
      • 0.5 µm: 44
      • 1.0 µm: 0
    • Zone 4:
      • 0.3 µm: 353
      • 0.5 µm: 176
      • 1.0 µm: 44
  • Started Cleaning (3:16 pm)
  • Finished Cleaning (4:10 pm)
  • Post-cleaning (4:15 pm):
    • Zone 3:
      • 0.3 µm: 574
      • 0.5 µm: 265
      • 1.0 µm: 132
    • Zone 4:
      • 0.3 µm: 177
      • 0.5 µm: 44
      • 1.0 µm: 0

 

  521   Sun Feb 23 16:00:07 2025 Luke UpdateScripts/ProgramsRingheater modeling Update

These are some plots:

The first shows the convergence of the 02 mode reducing the size of the mesh. The second shows the the numerical error of the zernike.

The first is found by sweeping a parameter that changes the size of the mesh. The HR surface was set to half a cm for all values.

The second by taking the inner product of a zernike mode with its self and calculating its deviation from pi for varying fineness of the mesh.

  371   Fri May 31 19:37:47 2024 LukeUpdate Vacuum chamber Disassembly
[Luke, Aiden, Jon, Michel, Tyler] Work done: On Tuesday (5/28) we removed the RGA line with minimal difficulty. On Wednesday (5/29) we removed the turbo pump, which had a few bolts that we needed to cut. We borrowed a dremel with ceramic blades from the machine shop to help remove some of the bolts. On Thursday we moved the vacuum chamber onto the floor to check and resecure the heating band on the bottom of the vacuum chamber. We then relocated the posts the vacuum chamber rests on closer to the end of the table and reinstalled the chamber. The post’s height was also reduced from 2in to 1in. Current state of vacuum chamber: The vacuum chamber is currently reinstalled in its new position. Some of the parts on the table will be used in the assembly of the turbo pump and RGA lines with the others being able to be moved to storage.
  378   Wed Jun 19 18:45:14 2024 LukeUpdate Vacuum chamber reassembly
[Luke, Aiden, Mohak , Tyler] On Tuesday we had the silver screws for the spherical cube shortened by a quarter of an inch so that they would fit into the gate valve. We then attached the spherical cube to the vacuum chamber. On Wednesday we finished assembling the RGA line and the main turbo pump.
  384   Tue Jun 25 17:19:42 2024 LukeUpdateVACVacuum chamber leak checking
Currently our main leak is in the RGA line. We found this by closing the gate valve from the main volume to see if which side was leaking more. After identifying this we are pumping down the main volume to see how low it can go the third attachment was taken at 4:16 6/25/24. Pumping started around 3:15. We have not been able to find exactly which flange is leaking, but our guess is on the small blanks and where the cube attaches to the gate valve as seen in the second attachment. We will try a few more things and if the leak is not found/fixed we are planning on changing the configuration of the RGA line to remove the spherical cube, which we believe to be the problem. See fourth attachment for rough sketch of initial idea. We have all of the parts required and they are clean and double bagged in 1129. I have not yet made all the measurements to confirm that this design is feasible.
  386   Wed Jun 26 16:39:34 2024 LukeUpdateVACVacuum chamber leak checking
On Tuesday I had isolated the main volume and let it pump down over-night. Today, Wednesday, I checked it and it had only gone down by a small amount compared to when I left it on Tuesday. I then proceeded to tighten down the bolts attaching the tubo-pump to the zero-length reducer while it was under vacuum. This caused the pressure to drop down a few orders of magnitude.
  390   Fri Jun 28 18:15:16 2024 LukeUpdateVACVacuum chamber

We will be configuring the RGA line to remove the spherical cube from the system. Currently our plan for the new design is to connect a 4.5" to 2.75" Reducing Cross to the gate valve on the vacuum system. It will be orientated vertically with the turbo pump on top coming off the end will be a 90 deg elbow. On the bottom there will be a 4.5" to 2.75" Zero length reducer attached to that will be a Tee on one side the pressure sensor and the other the RGA. Connected to the elbow will be the calibrated leak. 

The only parts not readily available are the ZLR and the 2.75" gaskets

Part name Count needed Status/comment
2.75" Tee 1 In use in current RGA line
4.5" to 2.75" Reducing Cross 1 Needs to be clean and baked
4.5" to 2.75" Zero length reducer 1 To be purchased  
2.75" 90 deg elbow 1 Clean needs to be removed from another part
5/16 - 24 X 2.00" Bolts and nuts 16

8 in clean room and plenty in storage they will need to be clean and baked. Plenty of nuts in clean room.

1/4 - 28 X 1.25" Bolts and nutplates 24 12 in use in RGA line and 12 in storage that will need to be clean and baked. Sufficient nutplates in clean room
1/4 - 28 X 7/8" Bolts  12 Plenty of bolts in clean room
2.75" Copper Gasket   6 5 gaskets in clean room and none in storage. So some will need to be purchased
4.5" Copper Gasket 2 About 10 in clean room 
  400   Wed Jul 10 17:31:07 2024 LukeUpdateVACRGA line disassembly and upgrade

[ Luke, Cynthia, Michael, Xuesi, Anthony ]

Started work around 12:45

We vented the chamber first and once it reached atmospheric pressure we started taking apart the RGA line.

We removed the parts in this order: Calibrated leak, RGA, Pressure gauge, 2.75" Blank on Tee, 2.75" Tee, all 1.33" Blanks on the cube, 4.5" feed through port, and finally the cube. Everything went smoothly after every part was taken off we covered the ends in Aluminum foil to maintain cleanliness. 

We then started the assembly of the new line. The parts were added in this order: Reducing cross, ZLR, Tee, Cal leak, RGA, 90 deg Elbow, and Pressure sensor.

We left off the Turbo pump as of now because we weren't able to find a 1" post not in use and we didn't want to put too much weight on the cross. We also noticed that the RGA might not fit on its probes because of a slight tilt to the cross and by extension the Tee. If this ends up being a problem we might need to remove all the parts connected to the cross so that we can reposition it so that the 2.75" rotating flange is connected to the gate valve.

Ended work around 4:00

  401   Thu Jul 11 15:53:39 2024 LukeUpdateVACRGA line upgrade

[ Luke, Jon ]

Started work at 11:00

As mentioned in my previous post the RGA was not clearing the table because of a tilt in the cross. So I removed the 90 deg elbow, loosened the bolt securing the Tee to the ZLR, and removed the cross from the gate valve. I then spun around the Tee on the bottom so that the cal leak would be pointing in the right direction and connected the rotating 2.75" flange of the cross to the gate valve. I then added the small turbo pump to the top of the cross. 

Then with the help of Dr. Richardson, we made some adjustments to how the Tee was oriented with respect to the cross and how the cross was with respect to the table. So that the cal leak and RGA would fit on the table. After that we made some changes to the bolting of the ZLR to reducing cross replacing the 2.00" bolts and nuts with 1.75" bolts and nut plates. We did face some difficulty with half of the 2.00" bolts which required a bit of torque to get them out. 

Finished work at 2:20 

 

Things to do:

Before we start pumping down the system again Dr. Richardson wanted two other changes to be made. To replace the 2.75" to 1.33" conical reducer with a zero length reducer. He also wants the bolts that hold the main turbo pump to be replaced with nut plates. 

I plan on starting this work on Friday (7/12) before pumping down over the weekend

  403   Sat Jul 13 15:09:04 2024 LukeUpdateGeneralRing heater COMSL model update

After the feedback from last meeting and Liu's help narrowing down what I should do to improve the model. I made some changes: First with Liu's help I made the proportions of the test mass and ring heater much more reasonable and parametrized by constants. Second from Cao's paper "FROSTI Nonimaging Reflector Design" Liu showed me what I should do to define the elliptical mirrors. Third during Friday's modeling/programming meeting walked me through getting the different irradiance plots to work. 

  411   Mon Jul 22 18:19:34 2024 LukeUpdateVACZero length reducer stuck bolts

Today, I borrowed a bolt extractor drill bit from the machine shop to remove some stuck bolts from the zlr. Before starting, I laid down a sheet of aluminum foil on the work table and wiped down all the tools I was going to use. I began by drilling a small pilot hole and then enlarged it with a 5/32 drill bit. However, when I attempted to use the bolt extractor, it didn't grip the bolt effectively. Our bolts were too seized, causing the extractor bit to repeatedly slip instead of gaining traction.

  427   Fri Aug 23 16:08:32 2024 LukeUpdateVACRGA line leak testing

[Luke, Luis, Jon, Tyler]

On the 22nd Dr. Richardson showed Luis, Tyler and I how to preform a leak test with the RGA. We did the initiall test and found a few leaks two were particuarly bad highlighted in orenge below. To try and remidy this we planned on replacing the copper gaskests on the leaking flanges. We then began taking the two problem flanges off, but seven of the eight bolts holding on the turbo pump were over tightened and had seized. So after we got them off we postponed the rest of the work to the next day.

On the 23nd Luis and I reattached the badly leaking flanges with new copper gaskets. We then preformed the Helium leak test with the RGA. As seen in the table below we weren't able to majorly changed the leaks in the two flanges.

 

Connection Initial  After disassembly
Tee - RGA 3.1e-9 -> 2.4e-9 9.2e-9
Tee - Cal leak Low Low
Tee - ZLR (2.75"-4.5") Low 9.2e-9
ZLR (2.75"-4.5") - Reducing Cross 2.1e-8 -> 1.9e-8 3.6e-8 -> 9.3e-9
Cross - Elbow Low 1.2e-9
Elbow - Pressure sensor Low 2.9e-9
Cross - Turbo pump (small) 2.1e-8 -> 3.1e-8 6.9e-8 -> 2.2e-8
Cross - Gate valve Low Low
Gate valve - Port 2.4e-9 -> 2.2e-9 1.2e-9
Port - ZLR (6.0"-8") 1.1e-9 N/A
ZLR (6.0"-8") - Turbo pump (large) Low N/A
Port - Pressure sensor Low N/A
Port - Up to air valve Low N/A
Port - Blank Low N/A
Port - Feed though  port Low N/A
Lid Low N/A

 

  429   Tue Aug 27 15:01:26 2024 LukeUpdateVACRGA line leak testing

[Luke, Tyler]

On the 27th Tyler and I ran the RGA leak test again with the electron multiplier on. These were the leaks we measured. The chamber's overall pressure was at ~6e-8 torr. 

Connection Leak rate (torr)
Tee - RGA 3.92e-11 (very low)
Tee - Cal leak 4.77e-11 (very low)
Tee - ZLR (2.75"-4.5") 4.97e-11 (very low)
ZLR (2.75"-4.5") - Reducing Cross 2.45e-9   (low)
Cross - Elbow 7.36e-11 (very low)
Elbow - Pressure sensor 2.36e-11 (very low)
Cross - Turbo pump (small) 8.07e-9   (lowish)
Cross - Gate valve 4.02e-11 (very low)
Gate valve - Port 2.27e-9   (low)
Port - ZLR (6.0"-8") 1.11e-9   (low)
ZLR (6.0"-8") - Turbo pump (large) 1.00e-10 (very low)
Port - Pressure sensor 1.05e-10 (very low)
Port - Up to air valve 1.08e-11 (very low)
Port - Blank 5.58e-10 (very low)
Port - Feed though port 1.21e-11 (very low)
Lid 1.11e-11 (very low)

 

 

  430   Tue Aug 27 18:37:40 2024 LukeUpdateInterferometer SimulationsRingheater model update
Updated the model to produce a more circular deformation in the HR surface. The first three attachments are from irradiance patterns gotten from ray tracing. The last is from a pre-defined irradiance pattern.
  431   Thu Aug 29 16:39:34 2024 LukeUpdateVACPhotos of heater tape
  432   Sun Sep 1 16:17:40 2024 LukeUpdateVACVacuum chamber leak checking and re-applying heating tape

[Luke, Luis, Cinthia, Michal, Tyler]

On the 26th Cinthia, Michal, and I took off the insolation on the vacuum chamber and re-routed it to include the new RGA volume. 

The next day Luis and I finished up the last of the flanges to be attached. We attached the Pirani gauge with a conical reducing nipple to the 2.75" port on the vacuum chamber. We then preformed the Helium leak testing, both flanges were quite low the 2.75" flange had a leak of 1.68e-10 torr and the 1.33" flange of 5.5e-12 torr. The leak on the 1.33" flange was so low it was difficult to know how much of it was real and how much was just noise.

  433   Tue Sep 3 15:52:56 2024 LukeUpdateVACHeater tape initilization

[Luke, Tyler, Jon]

On the 3rd we set up the pid controllers for the heater tapes and after putting on the insulation we started heating them up. We first brought it to ~50C and let it stabilize, there was about a 6-7 degree difference between the RGA and the barrel temperature, with the barrel being higher. We then brought it to 60 then 70C it still maintained the slight difference between the RGA and barrel temperatures.

Here is a table of the temperatures of the flanges connected to electronics as I left it.

Electronics Temperature (C)
Pressure gauge (Main volume) 58
Main turbo pump 45
RGA 37
Pressure gauge (RGA volume) 39
Cal leak 40
Mini tubo pump 36
Pirani gauge 37

Notes: I removed the electronics from the pressure gauge (main volume) because while it was below the required threshold it was still quite high compared to the other flanges.

  438   Mon Sep 9 21:02:37 2024 LukeUpdateVACSteadystate temperature of flanges

I measured the temperature of the flanges and reconnected the RGA turning on its filament. I then turned off the PID controllers.

Here is a table that has the temperature of the different parts of the vacuum chamber.

Electronics Temperature (C)
Pressure gauge (Main volume) 81
Main turbo pump 67
RGA 53
Pressure gauge (RGA volume) 60
Cal leak 48
Mini tubo pump 46
Pirani gauge (1.33") 46
conical nipple (2.75") 82
Lid 112
Barrel lower 125
Barrel upper 122
RGA volume 125
Bottom of chamber 117
  439   Mon Sep 16 07:28:16 2024 LukeUpdateInterferometer SimulationsRing heater update
  444   Mon Sep 23 08:29:49 2024 LukeUpdateInterferometer SimulationsRingheater update

Ringheater Update

If the link does not work here is the file.

  481   Sat Nov 30 12:41:42 2024 LukeUpdateVACVacuum bake end

The vacuum chamber has stopped bakeing. 

Current state as of 12:10, 11/30/2024:

The gate valve is open, and the filament of the RGA is on.

The temperatures were steady at:

PID right: barrel upper: 128°C,  RGA volume: 125°C

PID left: barrel lower: 125°C, Lid: 113°C

The RGA flange was 38°C

Cleanroom was 26°C

  493   Thu Dec 19 12:00:44 2024 LukeUpdateVACEnd of bake

The vacuum chamber has stopped baking. 

Current state as of 11:40, 12/19/2024:

The gate valve is open, and the filament of the RGA is on.

The temperatures were steady at:

PID right: barrel upper: 129°C,  RGA volume: 125°C

PID left: barrel lower: 125°C, Lid: 114°C

The RGA flange was 37°C

Cleanroom was 26°C

Note the upper barrel was very close to the emergency shut off temp of 130°C. In the future we may want to either rewire some of the heating tape or lower the set temperature of the right PID controller.

Luis and I are planning on taking an RGA scan of the MR on Sunday before the campus shuts down for the holidays.

  268   Thu Nov 16 17:12:42 2023 Luis, Shane, MohakUpdateCleanroomCleanroom cleaning and particle count
[Shane, Luis, Mohak]

cleaning cleanroom and particle count

  • 3:37 pm: started particle count
    • zone 3:
      • 0.3 u: 1205
      • 0.5 u: 748
      • 1.0 u: 249
    • zone 4:
      • 0.3 u: 1496
      • 0.5 u: 748
      • 1.0 u: 290
  • 3:57 pm: began surface check and wipedown, including softwalls. NOTE: vacuum chamber insulation crumbling at edges, dropping loose flakes. Scatters residue whenever jostled, so wiping it down just releases more. Not enough flakes are being released for it to be a major issue, but definitely something to keep an eye on.
  • 4:18 pm: started vacuuming the floor
  • 4:29 pm: finished vacuuming the floor
  • 4:30 pm: started mopping the floor
  • 4:35 pm: finished mopping the floor
  • 4:36 pm: started cleaning the buckets
  • 4:41 pm: started mopping with IPA wipes
  • 4:52 pm: finished mopping with IPA wipes
  • 4:52 pm: changed sticky floor mats
  • 4:53 pm: started particle count
    • zone 3:
      • 0.3 u: 3367
      • 0.5 u: 1787
      • 1.0 u: 914
    • zone 4:
      • 0.3 u: 1039
      • 0.5 u: 498
      • 1.0 u: 249
  425   Fri Aug 16 12:51:46 2024 Luis MartinUpdateVACUpdate on vacuum chamber status

[Luis, Luke, Tyler]

Vacuum chamber parts were finally received and assembled. After whipping down the parts, the blank was removed from the reducing cross. Then, the zero-length reducer was attached. Lastly, we installed the T that had the argon leak and RGA. The final pump down showed signs of an improved seal since the pressure dropped quite fast. This pressure is well bellow the limit required to use the RGA, argon test leak could be performed some time next week.

  440   Mon Sep 16 13:51:23 2024 Luis MartinUpdateVACRGA Scans

[Luis, Luke}

Three RGA scans were taken. The improvement in the amount of HC in the vacuum is visible across the different measurements. Images are attached.

  448   Wed Sep 25 09:06:09 2024 Luis MartinUpdateVACRGA Scans
RGA Scan Comparison

The following images compare the RGA scans from 9/23/24, after the first bake with the new vacuum system, with those from 3/14/24, after bake 12 with the old system.

The first image shows a graph of the raw data and includes the calibrated leak for both curves. As we can see, our new system meets LIGO standards of cleanliness.

The second graph contains the plot of the normalized data.

  459   Wed Oct 16 13:58:59 2024 Luis MartinUpdateVACRGA Scan

The following figure displays data acquired on 10/09, and it shows that we are no longer below the cleanliness standard. Also, the system's pressure went up to 1.9x10-8 Torr (approximately 7x10-9 Torr previously). This might be due to a leak somewhere in the system. More tests will be performed later.

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